U.S. Nuclear Regulatory Commission Operations Center Event Reports For 09/09/98 - 09/10/98 ** EVENT NUMBERS ** 34510 34746 34747 34753 34754 34755 34756 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 34510 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: VERMONT YANKEE REGION: 1 |NOTIFICATION DATE: 07/14/98 | |UNIT: [1] [ ] [ ] STATE: VT |NOTIFICATION TIME: 16:32 [ET]| |RX TYPE: [1] GE-4 |EVENT DATE: 07/14/98 | +------------------------------------------------+EVENT TIME: 16:14[EDT]| |NRC NOTIFIED BY: MICHAEL EMPEY |LAST UPDATE DATE: 09/09/98 | |HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |PETER ESELGROTH RDO | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE IDENTIFIED A SERVICE WATER ALIGNMENT, FOLLOWING A POSTULATED | | SERVICE WATER DISCHARGE LINE BREAK, THAT WAS NOT SUPPORTED BY ANY | | CALCULATIONS FOR RIVER WATER TEMPERATURES >45øF. | | | | THE FOLLOWING TEXT IS A PORTION OF A FACSIMILE RECEIVED FROM THE LICENSEE: | | | | "DURING A DESIGN BASIS DOCUMENTATION REVIEW OF THE SERVICE WATER SYSTEM, IT | | WAS DETERMINED THAT A CALCULATION DOES NOT EXIST TO SUPPORT THE FOLLOWING | | CONDITION: SHIFTING SERVICE WATER DISCHARGE TO THE COOLING TOWER DEEP | | BASIN FOR A PIPE BREAK DOWNSTREAM [OF] SERVICE WATER VALVE 18 (REACTOR | | BUILDING DISCHARGE ISOLATION) WITH RIVER TEMPERATURES >45øF PER FSAR | | SECTION 10.6.6." | | | | "AN INITIAL OPERABILITY DETERMINATION CONCLUDED [THAT] THE SYSTEM IS | | OPERABLE, AND A BASES FOR MAINTAINING OPERABILITY (BMO) WILL BE ISSUED." | | | | THE LICENSEE PLANS TO INFORM THE STATE INSPECTOR AND HAS INFORMED THE NRC | | RESIDENT INSPECTOR. | | | | * * * UPDATE AT 1649 ON 08/10/98 BY JIM BROOKS TO JOLLIFFE * * * | | | | THE LICENSEE PERFORMED A DETAILED ASSESSMENT OF PLANT OPERATING PROCEDURES, | | CURRENT LICENSING BASES, SERVICE WATER COOLING REQUIREMENTS AND FLOW | | CAPABILITIES, AND INTERVIEWS WITH PLANT OPERATING PERSONNEL. AFTER THIS | | ASSESSMENT, THE LICENSEE CONCLUDED THAT EXISTING PLANT PROCEDURES AND | | OPERATOR TRAINING ENSURE THAT THE EDGs (COMPONENTS OF CONCERN) WILL NOT | | BE LOADED TO A POINT WHERE THE EDGs WOULD NOT BE ADEQUATELY COOLED. THE | | LICENSEE FURTHER CONCLUDED THAT ACTIONS WOULD BE TAKEN TO MITIGATE ANY REAL | | OR POTENTIAL OVERHEATING OF THE EDGs AND ASSURE FLOW TO ESSENTIAL SERVICE | | WATER COOLING LOADS SHOULD THE SW-18 VALVE BE CLOSED WITH THE RIVER WATER | | TEMPERATURE HIGHER THAN 45øF. THE LICENSEE ALSO CONCLUDED THAT CONTINUED | | PLANT OPERATION WITHOUT ANY COMPENSATORY MEASURES IS ACCEPTABLE AND | | CONSISTENT WITH THE PLANT DESIGN BASES, AND THUS, THE LICENSEE DESIRES | | TO RETRACT THIS EVENT. | | | | THE LICENSEE PLANS TO INFORM THE NRC RESIDENT INSPECTOR. | | | | THE NRC OPERATIONS OFFICER NOTIFIED THE R1DO DAVE SILK. | | | | * * * UPDATE 1557 9/9/98 FROM SOLO TAKEN BY STRANSKY * * * | | | | THE FOLLOWING TEXT WAS SUBMITTED TO THE NRC OPERATIONS CENTER AT THE | | REQUEST OF THE RESIDENT INSPECTOR: | | | | "Update/Clarification: | | | | The following ENS notification was made on 7/14/98 (Event Number 34510) and | | updated (retracted) on 8/10/98. The retraction caused some concern because | | the basis for that retraction was not well documented. | | | | The retraction simply communicated the conclusion in the Basis for | | Maintaining Operation (BMO). The BMO concluded that continued operation was | | allowed without any compensatory measures. However the full scope of the | | BMO was not captured in the basis for the ENS notification retraction. The | | original ENS notification was made identifying that the plant had been | | potentially operating outside of its design basis because it could not be | | shown that operator actions which the FSAR describes as appropriate for | | isolation of a seismic Service Water discharge header would support | | Emergency Diesel Generator operation. | | | | The BMO documented the logic which adequately demonstrated that the EDG's | | would be provided with adequate cooling to perform their design functions | | were the plant operating crew to isolate the postulated breach as described | | in the FSAR. | | | | The BMO documented two basic conclusions. | | | | Firstly, that it is not necessary to assume accident mitigation loads on | | the EDG's coincident with the postulated piping breach. To postulate the | | spontaneous failure of a seismic line (a passive component) coincident with | | an accident initiator is inconsistent with VY's current licensing basis. | | However, VY has verified that accident mitigation loads can be supported by | | the EDG's with a concurrent failure of non-seismic branch lines connected | | to the Service Water supply header, with the Service Water header realigned | | as described in the FSAR | | | | Secondly, VY evaluated the ability of the EDG's to perform their safety | | functions in the event of a loss of off-site power with the postulated pipe | | break downstream of the SW-18 valve which could result in the SW discharge | | being rerouted to the cooling tower basin. It was recognized that the heat | | load on the EDG heat exchangers would be less absent the accident | | mitigation loads. It was concluded that existing plant procedures, and | | operator training, would ensure that the EDG's would not be loaded to the | | point where the EDG's would trip due to overheating. It was further | | concluded that actions would adequately mitigate any real or potential | | overheating of the EDG's and assure sufficient flow to essential SW cooling | | loads should the SW-18 valve be closed with the river temperature greater | | than 45F. | | | | It was also verified that Service Water Pump runout was not a problem in | | the alternate alignment." | | | | NOTIFIED R1DO (COSTELLO) | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 34746 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 09/07/98 | |UNIT: [1] [2] [ ] STATE: NY |NOTIFICATION TIME: 13:40 [ET]| |RX TYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 09/07/98 | +------------------------------------------------+EVENT TIME: 13:00[EDT]| |NRC NOTIFIED BY: FRANK SIENCZAK |LAST UPDATE DATE: 09/09/98 | |HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |DAVID LEW RDO | |AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | 2 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NATIONAL WEATHER SERVICE TONE ALERT RADIO SYSTEM INOPERABLE | | | | The National Weather Service tone alert radio system, which is part of the | | prompt notification system, was declared out of service as a result of a | | severe thunderstorm. This system serves a small portion of the population | | within the 10 mile EPZ. All prompt notification system sirens have been | | tested and are available. Additionally, the paging system used to notify | | the Site Emergency Response Organization is out of service due to the same | | thunderstorm. The telephone notification system is available to notify the | | Site Emergency Response Organization. | | | | The NRC resident inspector will be informed of this event by the licensee. | | | | * * * Update 1453 9/7/98 from Sienczak taken by Stransky * * * | | | | At 1410, the Oswego County reception center was declared out of service due | | to storm damage to the New York State Fairgrounds, where the center is | | located. The licensee is working with the county to develop compensatory | | actions. The NRC resident inspector will be informed. Notified R1DO (Lew). | | | | * * * Update 0522 9/9/98 from John Webers taken by MacKinnon * * * | | | | The National Weather Service tone alert radio system is now back in | | service. The NRC resident inspector was notified of this update. R1DO (Lew) | | notified. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 34747 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 09/07/98 | |UNIT: [1] [ ] [ ] STATE: NY |NOTIFICATION TIME: 13:51 [ET]| |RX TYPE: [1] GE-4 |EVENT DATE: 09/07/98 | +------------------------------------------------+EVENT TIME: 13:00[EDT]| |NRC NOTIFIED BY: NICK AVRAKOTOS |LAST UPDATE DATE: 09/09/98 | |HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |DAVID LEW RDO | |AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NATIONAL WEATHER SERVICE TONE ALERT RADIO SYSTEM INOPERABLE | | | | The National Weather Service tone alert radio system, which is part of the | | prompt notification system, was declared out of service as a result of a | | severe thunderstorm. This system serves a small portion of the population | | within the 10 mile EPZ. All prompt notification system sirens have been | | tested and are available. Additionally, the paging system used to notify | | the Site Emergency Response Organization was out of service due to the same | | thunderstorm, but has since been returned to service. The telephone | | notification system is also available to notify the Site Emergency Response | | Organization. | | | | The NRC resident inspector has been informed of this event by the licensee. | | | | * * * Update 1440 9/7/98 from Avrakotos taken by Stransky * * * | | | | At 1410, the Oswego County reception center was declared out of service due | | to storm damage to the New York State Fairgrounds, where the center is | | located. The licensee is working with the county to develop compensatory | | actions. The NRC resident inspector will be informed by the licensee. | | Notified R1DO (Lew). | | | | * * * Update at 1454 on 09/09/98 from Avrakotos to Trocine * * * | | | | Emergency Plan issues associated with the thunderstorms have been resolved. | | Reception at the New York State Fairgrounds has been returned to service. | | Following initial cleanup and utility and governmental emergency management | | operability reviews, the tone alert system was also returned to service. | | | | The licensee plans to notify the NRC resident inspector and the State. The | | county was involved in the assessment. The NRC Operations Officer notified | | the R1DO (Lew). | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 34753 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: FARLEY REGION: 2 |NOTIFICATION DATE: 09/09/98 | |UNIT: [1] [ ] [ ] STATE: AL |NOTIFICATION TIME: 08:14 [ET]| |RX TYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 09/09/98 | +------------------------------------------------+EVENT TIME: 05:16[CDT]| |NRC NOTIFIED BY: VAUDY HOLLEY |LAST UPDATE DATE: 09/09/98 | |HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |JOHN ZEILER RDO | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | A/R Y 100 POWER OPERATION | 0 HOT STANDBY | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 1 EXPERIENCED A TURBINE TRIP/REACTOR TRIP FROM 100% POWER FOR REASONS | | UNKNOWN. | | | | AT 0516CDT ON 9/9/98 UNIT 1 EXPERIENCED A TURBINE TRIP/REACTOR TRIP FOR | | REASONS UNKNOWN. ALL CONTROL RODS FULLY INSERTED. APPROXIMATELY 20 | | SECONDS FOLLOWING THE TRIP BOTH STEAM DRIVEN MAIN FEEDWATER PUMPS ALSO | | TRIPPED. THERE WAS NO MAINTENANCE OR TESTING IN PROGRESS AT THE TIME. ALL | | THREE AUXILIARY FEEDWATER PUMPS AUTOSTARTED AS EXPECTED AND THE UNIT IS | | CURRENTLY STABLE IN MODE 3 REJECTING DECAY HEAT TO THE MAIN CONDENSER VIA | | THE STEAM DUMPS. NO PRIMARY OR SECONDARY RELIEFS/SAFETIES LIFTED DURING | | THE TRANSIENT. ALSO, NO ELECTRICAL FAULTS WERE OBSERVED. THE LICENSEE IS | | CONDUCTING A ROOT CAUSE INVESTIGATION AND HAS INFORMED THE NRC RESIDENT | | INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 34754 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 09/09/98 | |UNIT: [1] [ ] [ ] STATE: MN |NOTIFICATION TIME: 08:52 [ET]| |RX TYPE: [1] GE-3 |EVENT DATE: 09/09/98 | +------------------------------------------------+EVENT TIME: 05:30[CDT]| |NRC NOTIFIED BY: DUANE VISTODEAU |LAST UPDATE DATE: 09/09/98 | |HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |JIM GAVULA RDO | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | M/R Y 60 POWER OPERATION | 0 HOT SHUTDOWN | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT WAS MANUALLY SCRAMMED FROM 60% POWER FOLLOWING A LOSS OF CONDENSER | | VACUUM. | | | | ALL FOUR SUCTION VALVES FROM THE MAIN CONDENSER TO THE STEAM JET AIR | | EJECTORS (SJAEs) WENT CLOSED FOR REASONS UNKNOWN. AN OFFGAS SYSTEM HIGH | | PRESSURE (10 PSI) ALARM WAS RECEIVED. OPERATORS RESPONDED BY DROPPING LOAD | | AND REDUCING RECIRCULATION FLOW. AT APPROXIMATELY 55-60% POWER A MANUAL | | REACTOR SCRAM WAS INITIATED. ALL CONTROL RODS FULLY INSERTED. NO | | SRVs/SAFETIES LIFTED DURING THE TRANSIENT. A GROUP 2 (PRIMARY CONTAINMENT) | | AND 3 (RWCU) ISOLATION OCCURRED WHICH HAVE BEEN RESET. THE UNIT IS | | CURRENTLY STABLE IN HOT SHUTDOWN WITH ONE REACTOR FEED PUMP IN SERVICE WITH | | DECAY HEAT BEING REJECTED TO THE MAIN CONDENSER. THERE IS SUFFICIENT | | LEAKBY ON THE CLOSED SUCTION VALVES TO THE SJAEs TO MAINTAIN CONDENSER | | VACUUM. ALL ECCS EQUIPMENT IS AVAILABLE IF NEEDED. THE LICENSEE NOTIFIED | | THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |OTHER NUCLEAR MATERIAL | |EVENT NUMBER: 34755 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |LICENSEE: US ARMY (ACALA) |NOTIFICATION DATE: 09/09/98 | | CITY: DUGWAY PROVING REGION: 4 |NOTIFICATION TIME: 14:02 [ET]| | COUNTY: TOOELE STATE: UT |EVENT DATE: 09/09/98 | |LICENSE#: 12-00722 AGREEMENT: Y |EVENT TIME: 00:00[MDT]| | DOCKET: |LAST UPDATE DATE: 09/09/98 | | +-----------------------------+ | |PERSON ORGANIZATION| | |JIM GAVULA RDO | | |STEVE BAGGETT EO | +------------------------------------------------+ | |NRC NOTIFIED BY: TIM MOHS | | |HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: NOT APPLICABLE | | |10 CFR SECTION: | | |IBAC 30.50(b)(1)(i) ACCESS DENIED >24 HRS | | | | | | | | | | | | | | +------------------------------------------------+-----------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ACCESS TO STORAGE AREA RESTRICTED DUE TO TRITIUM CONTAMINATION | | | | ON 9/2/98, A REPRESENTATIVE OF THE ARMAMENT AND CHEMICAL ACQUISITION AND | | LOGISTICS ACTIVITY (ACALA) VISITED THE DUGWAY PROVING GROUNDS IN UTAH TO | | PERFORM WIPE TESTS ON TRITIUM FILLED FIRE CONTROL EQUIPMENT. DURING HIS | | VISIT, THE ACALA REPRESENTATIVE BECAME AWARE THAT BROKEN DEVICES WERE BEING | | STORED IN A ROOM WITH MORTARS. BECAUSE OF THE POSSIBILITY OF CONTAMINATION, | | MORTAR TESTING WAS SUSPENDED PENDING THE RESULTS OF THE WIPE TESTS. | | | | ON 9/8/98, RESULTS OF SCINTILLATION COUNTS OF THE WIPE SAMPLES WERE | | RECEIVED. SEVERAL ITEMS WERE FOUND TO HAVE VERY HIGH LEVELS OF TRITIUM | | CONTAMINATION (WIPES RANGED FROM SEVERAL THOUSAND DPM TO 1.2 MILLION DPM). | | ACCESS TO THE STORAGE ROOM HAS BEEN RESTRICTED PENDING DECONTAMINATION OF | | EQUIPMENT. SOME OF THE MORE CONTAMINATED ITEMS HAVE BEEN PLACED IN DOUBLE | | PLASTIC BAGS AND STORED IN DRUMS. THE US ARMY PLANS TO LOOK FOR | | CONTAMINATION IN AREAS OUTSIDE OF THE STORAGE AREA AND WILL TAKE ANY | | APPROPRIATE ACTIONS. | | | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 34756 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 09/09/98 | |UNIT: [1] [2] [ ] STATE: FL |NOTIFICATION TIME: 15:22 [ET]| |RX TYPE: [1] CE,[2] CE |EVENT DATE: 09/08/98 | +------------------------------------------------+EVENT TIME: 00:00[EDT]| |NRC NOTIFIED BY: WEINKAM |LAST UPDATE DATE: 09/09/98 | |HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |JOHN ZEILER RDO | |NONR OTHER UNSPEC REQMNT | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | 2 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 72-HOUR NOTIFICATION OF UNUSUAL OR IMPORTANT ENVIRONMENTAL EVENT | | | | ON 9/8/98, THE LICENSEE OBSERVED AN INCREASE IN NUISANCE ORGANISMS (LARGE | | NUMBERS OF JELLYFISH) IN THE PLANT INTAKE CANAL. THE LICENSEE REDUCED POWER | | OF UNIT 2 IN ANTICIPATION OF SIGNIFICANT BLOCKAGE OF THE CIRCULATING WATER | | SYSTEM. NO SIGNIFICANT BLOCKAGE ACTUALLY OCCURRED, AND UNIT 2 WAS RESTORED | | TO FULL POWER ON 9/9/98. THE LICENSEE PERFORMED AN AERIAL SURVEY OF THE | | INTAKE CANAL AND OCEAN IN THE VICINITY OF THE PLANT, BUT NO ADDITIONAL | | JELLYFISH CLUSTERS WERE OBSERVED. | | | | THIS REPORT WAS MADE IN ACCORDANCE WITH SECTION 4.1 OF THE ST. LUCIE | | ENVIRONMENTAL PROTECTION PLAN. THE NRC RESIDENT INSPECTOR HAS BEEN | | INFORMED. | +------------------------------------------------------------------------------+