U.S. Nuclear Regulatory Commission Operations Center Event Reports For 03/09/98 - 03/10/98 ** EVENT NUMBERS ** 33669 33861 33862 33863 33864 33865 33866 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 33669 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 02/06/98 | |UNIT: [ ] [2] [ ] STATE: NY |NOTIFICATION TIME: 13:30 [ET]| |RX TYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 02/06/98 | +------------------------------------------------+EVENT TIME: 12:30[EST]| |NRC NOTIFIED BY: ORZELL |LAST UPDATE DATE: 03/09/98 | |HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |LAURIE PELUSO RDO | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | 2 | N Y 95 POWER OPERATION | 95 POWER OPERATION | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | VIOLATION OF CABLE SEPARATION CRITERIA. | | | | DURING A PLANT WALKDOWN, THE RESIDENT INSPECTOR DISCOVERED THAT FLEX | | CONDUIT FROM "RHS*TE49A" WAS TOUCHING THE FLEX CONDUIT OF "RHS*TE49B". | | THE TEMPERATURE ELEMENTS PROVIDE FOR GROUPS 5 & 10 ISOLATION, RHR SHUTDOWN | | COOLING ISOLATION, AND SYSTEM RCIC ISOLATION. ENGINEERING SPECIFICATION | | "E61A" STATES THAT MINIMUM DISTANCE BETWEEN ENCLOSED RACEWAY OF DIFFERENT | | COLORS (DIV 1 & DIV 2) SHOULD BE 1/2 INCH. THE CONDITION OBSERVED DID NOT | | MEET THIS CRITERIA, AND WAS DETERMINED TO BE OUTSIDE THE DESIGN BASIS. | | THE AFFECTED INSTRUMENTS WERE ALSO DECLARED INOPERABLE, HOWEVER, THEY WERE | | RETURNED TO OPERABLE STATUS AT 1315 WHEN THE SEPARATION CRITERIA WAS MET. | | | | THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR. | | | | * * * UPDATE AT 1604 ON 03/09/98 BY DON NEWMAN ENTERED BY JOLLIFFE * * * | | | | BASED ON FURTHER EVALUATION, THE LICENSEE DETERMINED THAT THE FUNCTION OF | | THE TEMPERATURE ELEMENTS (TEs) WAS NOT IMPACTED BY THE CONDUITS TOUCHING | | (i.e., EVEN THOUGH THE CONDUITS FOR THE 'A' AND 'B' TRAIN TEs WHOSE | | CONDUITS WERE TOUCHING COULD HAVE BEEN NEGATIVELY AFFECTED, THE 'C' AND 'D' | | TRAIN TEs WHOSE CONDUITS WERE NOT TOUCHING WOULD NOT HAVE BEEN NEGATIVELY | | AFFECTED). THUS, ALTHOUGH THIS CONDITION WAS A DEVIATION FROM THE | | SEPARATION REQUIREMENTS, IT WAS NOT A CONDITION THAT WAS OUTSIDE THE DESIGN | | BASIS OF THE PLANT. THEREFORE, THE LICENSEE DESIRES TO RETRACT THIS EVENT. | | THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR. THE OPERATIONS | | OFFICER NOTIFIED THE R1DO RICH CONTE. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 33861 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: FARLEY REGION: 2 |NOTIFICATION DATE: 03/08/98 | |UNIT: [1] [2] [ ] STATE: AL |NOTIFICATION TIME: 23:41 [ET]| |RX TYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 03/08/98 | +------------------------------------------------+EVENT TIME: 22:00[CST]| |NRC NOTIFIED BY: VAUDY HOLLY |LAST UPDATE DATE: 03/09/98 | |HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: UNUSUAL EVENT +-----------------------------+ |10 CFR SECTION: |CAUDLE JULIAN RDO | |AAEC 50.72(a)(1)(i) EMERGENCY DECLARED |STUART RICHARDS, NRR EO | | |FRANK CONGEL, AEOD IRD | | |CHUCK DePUY FEMA | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | 2 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DECLARATION OF UNUSUAL EVENT DUE TO FLOODING OF THE CHATTAHOOCHEE RIVER AND | | INABILITY TO ACCESS THE INTAKE STRUCTURE VIA NORMAL MEANS. | | | | THE AREA IS CURRENTLY EXPERIENCING HEAVY RAINS, AND FLOODING IS OCCURRING | | ON THE CHATTAHOOCHEE RIVER. THE RIVER WATER LEVEL IS CURRENTLY 113.4 FEET | | AND INCREASING. THE RISING RIVER WATER LEVEL AND HEAVY RAINS HAVE | | INHIBITED THE LICENSEE'S ABILITY TO ACCESS THE INTAKE STRUCTURE BY | | AUTOMOBILE. THE LICENSEE STATED THAT BOATS ARE AVAILABLE. BECAUSE NORMAL | | ACCESS CANNOT BE GAINED TO AN OUT BUILDING, THE LICENSEE DECLARED AN | | UNUSUAL EVENT AT 2200 CST. THE LICENSEE STATED THAT NORMAL PLANT | | OPERATIONS ARE NOT AFFECTED. | | | | (NOTE: THE RIVER IS NOT THE ULTIMATE HEAT SINK FOR THIS SITE.) | | | | BOTH HOUSTON COUNTY, ALABAMA AND EARLY COUNTY, GEORGIA HAVE CONFIRMED | | THAT THE ROADS WITHIN THE 10-MILE EMERGENCY PLANNING ZONE HAVE NOT BEEN | | AFFECTED, AND EVACUATION OF LOCAL PERSONNEL COULD STILL BE PERFORMED, IF | | NECESSARY. THE LICENSEE PLANS TO TERMINATE THE UNUSUAL EVENT WHEN NORMAL | | ACCESS TO THE INTAKE STRUCTURE IS REGAINED. | | | | THE LICENSEE NOTIFIED THE STATES OF ALABAMA AND GEORGIA AND HOUSTON AND | | EARLY COUNTIES. THE LICENSEE ALSO PLANS TO NOTIFY THE NRC RESIDENT | | INSPECTOR. | | | | * * * UPDATE AT 1205 ON 03/09/98 FROM BOB VANDERBYE TAKEN BY BAILEY * * * | | | | THE LICENSEE REPORTED THAT THEY WERE ACTUALLY ABLE TO ACCESS THE INTAKE | | STRUCTURE BY TRUCKS UNTIL 0930 CST ON 03/09/98. HOWEVER, AS OF 0930 CST, | | THEY ARE ACCESSING THE INTAKE STRUCTURE ONLY BY BOAT. AT 1105 CST, THE | | RIVER LEVEL WAS 115 FEET, 6 INCHES AND RISING AT THE RATE OF 1-2 INCHES PER | | HOUR. AN ESTIMATE OF THE RIVER CRESTING LEVEL AND TIME IS EXPECTED FROM | | THE ARMY CORPS OF ENGINEERS TODAY. THE FLOOD LEVEL IS 112 FEET. THE | | DESIGN BASIS LEVEL IS 126 FEET. BOTH COUNTIES CAN STILL EVACUATE | | PERSONNEL, IF NECESSARY. | | | | THE LICENSEE NOTIFIED THE NRC RESIDENT INSPECTOR. | | | | THE NRC OPERATIONS OFFICER NOTIFIED THE R2DO CAUDLE JULIAN. | | | | * * * UPDATE AT 1657 ON 03/09/98 FROM BOB VANDERBYE TAKEN BY JOLLIFFE * * * | | | | THE CORPS OF ENGINEERS REPORTED TO THE LICENSEE THAT THE CHATTAHOOCHEE | | RIVER IS EXPECTED TO CREST BETWEEN 116 FEET, 2 INCHES AND 116 FEET, | | 8 INCHES PRIOR TO 0700 ON 03/10/98. | | | | THE LICENSEE PLANS TO NOTIFY STATE AND COUNTY OFFICIALS AND THE NRC | | RESIDENT INSPECTOR. | | | | THE NRC OPERATIONS OFFICER NOTIFIED THE R2DO CAUDLE JULIAN. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 33862 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: BROWNS FERRY REGION: 2 |NOTIFICATION DATE: 03/09/98 | |UNIT: [ ] [2] [ ] STATE: AL |NOTIFICATION TIME: 00:14 [ET]| |RX TYPE: [1] GE-4,[2] GE-4,[3] GE-4 |EVENT DATE: 03/08/98 | +------------------------------------------------+EVENT TIME: 20:56[CST]| |NRC NOTIFIED BY: RAYMOND SWAFFORD |LAST UPDATE DATE: 03/09/98 | |HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |CAUDLE JULIAN RDO | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | 2 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 2 EXPERIENCED A HALF-SCRAM AND VARIOUS GROUP ISOLATIONS DUE TO A | | DEFICIENT CLEARANCE ASSOCIATED WITH PLANNED MAINTENANCE ON THE '2B' REACTOR | | PROTECTION SYSTEM MOTOR GENERATOR (RPS MG) SET. | | | | "AT 2056 CST ON 3/8/98, BROWNS FERRY NUCLEAR PLANT-TVA (UNIT 2) RECEIVED A | | HALF-SCRAM AND THE FOLLOWING ISOLATIONS: GROUPS 2, 3, 6, AND 8. ALL THREE | | TRAINS OF STANDBY GAS TREATMENT STARTED AS WELL AS CREV 'A' (CONTROL ROOM | | EMERGENCY VENTILATION TRAIN 'A'). | | | | "[THE] '2B' RPS HAD BEEN TRANSFERRED TO ITS ALTERNATE SUPPLY IN PREPARATION | | FOR MAINTENANCE ON THE '2B' RPS MG SET. THE '2B' RPS MG SET IS THE NORMAL | | SUPPLY TO [THE] '2B' RPS, AND HAD BEEN SHUTDOWN AFTER THE TRANSFER. AT | | 2056 CST ON 3/8/98, BROWNS FERRY NUCLEAR PLANT-TVA RECEIVED A '2B' | | HALF-SCRAM AND ALL THE EXPECTED ASSOCIATED ISOLATIONS AND ACTUATIONS AS | | STATED ABOVE. INVESTIGATION INTO THE CAUSE REVEALED THAT AS OPERATIONS | | PERSONNEL WERE HANGING THE CLEARANCE IN PREPARATION FOR THE MAINTENANCE | | WORK, ONE OF THE HOLD ORDER CARDS ERRONEOUSLY HAD THE REQUIRED POSITION FOR | | THE NORMAL/ALTERNATE HANDSWITCH TO BE IN ITS NORMAL POSITION. WHEN THE | | HANDSWITCH WAS TAKEN TO NORMAL, THIS IN ESSENCE TRANSFERRED [THE] '2B' RPS | | TO A DEAD BUS. | | | | "THIS IS REPORTABLE VIA ENS AS A 4-HOUR REPORT AS 'ANY EVENT OR CONDITION | | THAT RESULTS IN MANUAL...ACTUATION OF ANY ENGINEERED SAFETY FEATURE (ESF) | | INCLUDING THE REACTOR PROTECTION SYSTEM (RPS)." | | | | ALL ISOLATIONS AND ACTUATIONS HAVE BEEN RESET. THE LICENSEE INFORMED THE | | NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 33863 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: COMANCHE PEAK REGION: 4 |NOTIFICATION DATE: 03/09/98 | |UNIT: [ ] [2] [ ] STATE: TX |NOTIFICATION TIME: 01:14 [ET]| |RX TYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/08/98 | +------------------------------------------------+EVENT TIME: 22:01[CST]| |NRC NOTIFIED BY: ELIZABETH MEADERS |LAST UPDATE DATE: 03/09/98 | |HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |TOM STETKA RDO | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | 2 | A/R Y 100 POWER OPERATION | 0 HOT STANDBY | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 2 EXPERIENCED A REACTOR TRIP DUE TO THE LOSS OF THE TURBINE PLANT | | COOLING WATER SYSTEM. | | | | "AT APPROXIMATELY 2200 CST, BOTH TURBINE PLANT COOLING WATER (TPCW) PUMPS | | ON UNIT 2 TRIPPED DUE TO LO-LO LEVEL IN THE TPCW HEAD TANK. WHILE | | PERFORMING A 48-HOUR FEED AND BLEED ON THE TPCW SYSTEM, THE MAKEUP VALVE | | FOR THE HEAD TANK DID NOT AUTO OPEN AND NO ALARMS WERE RECEIVED IN THE | | CONTROL ROOM PRIOR TO REACHING THE LO-LO LEVEL SETPOINT DUE TO A LEVEL | | SWITCH FAILURE. THIS RESULTED IN A PRIMARY WATER HIGH TEMPERATURE TURBINE | | TRIP AND A CORRESPONDING AUTOMATIC REACTOR TRIP. | | | | "BOTH THE MOTOR DRIVEN (MDAFW) AND TURBINE DRIVEN (TDAFW) AUXILIARY | | FEEDWATER PUMPS STARTED DUE TO STEAM GENERATOR SHRINK FOLLOWING THE TRIP. | | THE TDAFW PUMP WAS TAKEN TO STOP BUT, DUE TO LO-LO SG LEVEL IN MORE THAN | | ONE SG, THE PUMP AUTOSTARTED AGAIN. THE PLANT WAS STABILIZED IN MODE 3 AND | | ALL SYSTEMS FUNCTIONED AS REQUIRED." | | | | ALL RODS FULLY INSERTED FOLLOWING THE REACTOR TRIP. NO PRIMARY OR | | SECONDARY SAFETY OR RELIEF VALVES LIFTED. DECAY HEAT IS BEING REJECTED VIA | | THE NORMAL STEAM DUMPS TO THE MAIN CONDENSER. THE FAILED LEVEL SWITCH | | NORMALLY OPENS THE MAKEUP VALVE AT 63% LEVEL AND CAUSES AN ALARM AT 6% | | LEVEL. OPERATORS TAKE TANK LEVEL READINGS EVERY SHIFT (12 HOURS) AND DID | | NOT OBSERVE LOWERING LEVEL INDICATION PRIOR TO THE TRIP. THE TPCW SYSTEM | | HAS BEEN RETURNED TO SERVICE WITH THE #2 TPCW PUMP OPERATING. THERE IS NO | | INDICATION OF ANY EQUIPMENT DAMAGE. THE LICENSEE INFORMED THE NRC RESIDENT | | INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 33864 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 03/09/98 | |UNIT: [1] [2] [ ] STATE: FL |NOTIFICATION TIME: 04:44 [ET]| |RX TYPE: [1] CE,[2] CE |EVENT DATE: 03/09/98 | +------------------------------------------------+EVENT TIME: 04:04[EST]| |NRC NOTIFIED BY: DON TALLEY |LAST UPDATE DATE: 03/09/98 | |HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |CAUDLE JULIAN RDO | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | 2 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT SECURITY EVENT - | | | | SAFEGUARDS SYSTEM DEGRADATION DUE TO ADVERSE WEATHER. THE LICENSEE WAS | | UNABLE TO IMPLEMENT COMPENSATORY ACTIONS WITHIN THE ALLOWED 10 MINUTES. | | COMPENSATORY MEASURES CURRENTLY IN PROGRESS. THE LICENSEE WILL INFORM THE | | NRC RESIDENT INSPECTOR. SEE HOO LOG FOR DETAILS. | | | | * * * UPDATE AT 0725 EST BY GARY VARNES TO S. SANDIN * * * | | | | THE LICENSEE REPORTED THAT COMPENSATORY MEASURES WERE FULLY IMPLEMENTED | | BY 0446 EST AND THAT SAFEGUARDS WAS REESTABLISHED AS OF 0640 EST. THE | | LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. THE OPERATIONS OFFICER | | NOTIFIED THE R2DO (CAUDLE JULIAN). | | | | * * * UPDATE AT 1528 BY DAVE WILLIAMS TO JOLLIFFE * * * | | | | THE LICENSEE DESIRES TO ALSO CLASSIFY THIS EVENT AS FOLLOWS: | | 10CFR50.54X AND Y, AND 10CFR50.72(b)(1)(i)(B). THE LICENSEE PLANS TO | | SUBMIT A WRITTEN REPORT ON THIS EVENT TO THE NRC. THE LICENSEE INFORMED | | THE NRC RESIDENT INSPECTOR. THE OPERATIONS OFFICER NOTIFIED THE R2DO | | (CAUDLE JULIAN). | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |GENERAL INFORMATION or OTHER | |EVENT NUMBER: 33865 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |LICENSEE: STATE OF FLORIDA |NOTIFICATION DATE: 03/09/98 | | CITY: ROCKLEDGE REGION: 2 |NOTIFICATION TIME: 14:54 [ET]| | COUNTY: STATE: FL |EVENT DATE: 03/09/98 | |LICENSE#: 1136-4 AGREEMENT: Y |EVENT TIME: 07:30[EST]| | DOCKET: |LAST UPDATE DATE: 03/09/98 | | +-----------------------------+ | |PERSON ORGANIZATION| | |CAUDLE JULIAN RDO | | | | +------------------------------------------------+FEMA, DOE, DOA, HHS FAX | |NRC NOTIFIED BY: CHARLES ADAMS-STATE OF FL |EPA, DOT (NRC) FAX | |HQ OPS OFFICER: DICK JOLLIFFE | | +------------------------------------------------+ | |EMERGENCY CLASS: NOT APPLICABLE | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------+-----------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - PORTABLE TROXLER MOISTURE DENSITY GAUGE STOLEN FROM A TRUCK - | | | | CHARLES ADAMS, STATE OF FLORIDA BUREAU OF RADIATION CONTROL, REPORTED THAT | | A PORTABLE TROXLER MOISTURE DENSITY GAUGE (MODEL #3411B, SERIAL #1163) | | CONTAINING TWO DOUBLE ENCAPSULATED SEALED SOURCES, 8 mCi Cs-137 AND 40 mCi | | Am-241/Be, WAS APPARENTLY STOLEN FROM A TRUCK OWNED BY UNIVERSAL | | ENGINEERING SCIENCES, INC, ROCKLEDGE, FL. THE GAUGE WAS SECURED BY CABLE | | TO THE TRUCK. THE TRUCK WAS PARKED AT AN EMPLOYEE'S RESIDENCE IN | | MELBOURNE, FL, ON 03/07/98 AND THE GAUGE WAS DISCOVERED MISSING AT 0730 ON | | 03/09/98. | | THE MELBOURNE POLICE DEPARTMENT IS INVESTIGATING THIS SITUATION. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 33866 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: VOGTLE REGION: 2 |NOTIFICATION DATE: 03/09/98 | |UNIT: [1] [2] [ ] STATE: GA |NOTIFICATION TIME: 15:01 [ET]| |RX TYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/09/98 | +------------------------------------------------+EVENT TIME: 11:40[EST]| |NRC NOTIFIED BY: DAVE McCARY |LAST UPDATE DATE: 03/09/98 | |HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |CAUDLE JULIAN RDO | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | 2 | N N 0 COLD SHUTDOWN | 0 COLD SHUTDOWN | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - FITNESS FOR DUTY EVENT - | | | | AT 1140 ON 03/09/98, THE LICENSEE WAS INFORMED OF A CONFIRMED POSITIVE | | RANDOM DRUG TEST RESULTS OF A LICENSEE PLANT EMPLOYEE SUPERVISOR. THE | | LICENSEE WITHDREW THE INDIVIDUAL'S PLANT ACCESS AUTHORIZATION AND IS | | INVESTIGATING THIS SITUATION INCLUDING REVIEWING THE INDIVIDUAL'S RECENT | | WORK ACTIVITIES. THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+