U.S. Nuclear Regulatory Commission Operations Center Event Reports For 10/05/98 - 10/06/98 ** EVENT NUMBERS ** 34842 34870 34872 34873 34874 34875 34876 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 34842 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: CATAWBA REGION: 2 |NOTIFICATION DATE: 09/27/98 | |UNIT: [1] [2] [ ] STATE: SC |NOTIFICATION TIME: 11:56 [ET]| |RX TYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 09/27/98 | +------------------------------------------------+EVENT TIME: 08:15[EDT]| |NRC NOTIFIED BY: MIKE FERGUSON |LAST UPDATE DATE: 10/05/98 | |HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |AL BELISLE RDO | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | 2 | N N 0 REFUELING | 0 REFUELING | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LICENSEE NOTIFIED FEDERAL AND STATE AGENCIES OF MINOR OIL SPILL. | | | | THE FOLLOWING TEXT IS A PORTION OF A FACSIMILE RECEIVED FROM THE LICENSEE: | | | | "AT 0815, DURING THE START OF THE 'A' MAIN FIRE WATER PUMP, APPROXIMATELY | | ONE TEASPOON OF OIL THAT HAD COLLECTED AROUND THE PUMP HOUSING/STRUCTURE | | WAS DISPLACED INTO WATERS OF LAKE WYLIE BENEATH THE PUMP STRUCTURE. | | DISPLACEMENT OF THIS OIL RESULTED IN AN OIL SHEEN THAT COVERED AN AREA OF | | FOUR INCHES BY FOUR FEET. OIL WAS EFFECTIVELY CONTAINED WITHIN THE | | IN-PLACE OIL BOOMS." | | | | "THE OIL SHEEN DISPERSED WITHIN 1 HOUR OF THE INITIAL SPILL. THERE IS NO | | ACTIVE OIL LEAK AT THIS TIME." | | | | "THIS NOTIFICATION IS BEING MADE PURSUANT TO 10 CFR 50.72(b)(2)(vi) DUE TO | | NOTIFICATION TO [THE] SOUTH CAROLINA DEPARTMENT OF HEALTH AND ENVIRONMENTAL | | CONTROL AND THE NATIONAL RESPONSE CENTER (REPORT #457312) BY CATAWBA | | NUCLEAR STATION ENVIRONMENTAL MANAGEMENT." | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | | | | * * * UPDATE AT 1700 EDT ON 10/05/98 FROM GARY HAMILTON TO S.SANDIN * * * | | | | THE LICENSEE IS RETRACTING THIS EVENT NOTIFICATION BASED ON THE FOLLOWING: | | | | "ON INVESTIGATION, NO SPILL OR OIL SHEEN COULD BE VERIFIED BY THE | | ENVIRONMENTAL PROFESSIONAL." | | | | "THERE HAS BEEN NO MAINTENANCE PERFORMED ON THE FIRE PUMPS SINCE FEBRUARY | | 1998; THERE WAS NO INITIATING EVENT SUCH AS A LEAKING VALVE OR SPILL; THE | | ONLY EVENT WAS NORMAL STARTUP OF A PUMP WITH NO VISIBLE OIL SHEEN EVIDENT | | UPON INVESTIGATION. THIS EVENT HAS BEEN RECALLED BOTH WITH THE SOUTH | | CAROLINA DEPARTMENT OF HEALTH AND ENVIRONMENTAL CONTROL AND THE NATIONAL | | RESPONSE CENTER. THIS EVENT WILL NOT COUNT AS A REPORTABLE SPILL EVENT." | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. THE NRC OPERATIONS | | OFFICER NOTIFIED THE R2DO (BOLAND). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 34870 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 10/03/98 | |UNIT: [1] [ ] [ ] STATE: IL |NOTIFICATION TIME: 18:32 [ET]| |RX TYPE: [1] GE-6 |EVENT DATE: 10/03/98 | +------------------------------------------------+EVENT TIME: 15:00[CDT]| |NRC NOTIFIED BY: R POWERS |LAST UPDATE DATE: 10/05/98 | |HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |GARY SHEAR RDO | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N N 0 COLD SHUTDOWN | 0 COLD SHUTDOWN | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AN UNEXPECTED ENGINEERED SAFETY FEATURE (ESF) ACTUATION OCCURRED WHEN A | | MAIN STEAM ISOLATION VALVE ABOVE-SEAT DRAIN CLOSED. | | | | DURING AN EVOLUTION TO TEMPORARILY LIFT A TAGOUT ON A PORTION OF THE MAIN | | STEAM SYSTEM FOR PERFORMANCE OF A LOCAL LEAK RATE TEST ON THE SYSTEM, THE | | 1B21-F067A VALVE (THE OUTBOARD MAIN STEAM ISOLATION VALVE ABOVE-SEAT DRAIN) | | WENT CLOSED WHEN THE BREAKER WAS TURNED ON. LOCAL POSITION INDICATION OF | | THE 1B21-F067A VALVE IS DIFFICULT TO DETERMINE DUE TO THE TYPE OF MOTOR | | OPERATOR. THE OPERATOR PERFORMING THE TEMPORARY LIFT BELIEVED THE | | 1B21-F067A VALVE TO BE CLOSED AND REMOVED THE DANGER TAG AFTER WHICH THE | | 1B21-F067A VALVE WENT CLOSED. THE CLOSURE OF THE 1B21-F067A VALVE WAS | | CAUSED BY A GROUP-1 CONTAINMENT AND REACTOR VESSEL CONTROL SYSTEM ISOLATION | | DUE TO LOW CONDENSER VACUUM. THE CONDENSER VACUUM SYSTEM IS CURRENTLY OUT | | OF SERVICE DUE TO CURRENT PLANT CONDITIONS. | | | | THE NRC RESIDENT INSPECTOR WAS NOTIFIED OF THIS EVENT BY THE LICENSEE. | | | | * * * UPDATE AT 1543 EDT ON 10/05/98 FROM ROBERT POWERS TO S.SANDIN * * * | | | | THE LICENSEE IS RETRACTING THIS EVENT NOTIFICATION BASED ON THE FOLLOWING: | | | | "PER NUREG-1022, REV. 1, THE ACTUATION OF [THE] 1B21-F067A [VALVE] DOES NOT | | MEET THE REPORTING REQUIREMENTS OF 10 CFR 50.72(b)(2)(ii). THIS EVENT IS | | NOT REPORTABLE BECAUSE IT CONSTITUTED THE INADVERTENT ACTUATION OF A SINGLE | | COMPONENT OF AN ESF SYSTEM RATHER THAN A TRAIN LEVEL ACTUATION AND | | [BECAUSE] THE PURPOSE OF THE ACTUATION DID NOT MITIGATE THE CONSEQUENCES OF | | AN EVENT." | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. THE NRC OPERATIONS | | OFFICER NOTIFIED THE R3DO (KOZAK). | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 34872 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 10/05/98 | |UNIT: [ ] [2] [ ] STATE: GA |NOTIFICATION TIME: 13:16 [ET]| |RX TYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 10/05/98 | +------------------------------------------------+EVENT TIME: 10:00[EDT]| |NRC NOTIFIED BY: BARRY COLEMAN |LAST UPDATE DATE: 10/05/98 | |HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |ANN BOLAND RDO | |AINA 50.72(b)(2)(iii)(A) POT UNABLE TO SAFE SD | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | 2 | N N 0 REFUELING | 0 REFUELING | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE DISCOVERED DURING CONTROL ROD DRIVE (CRD) TESTING THAT AN | | ELECTRICAL JUMPER INSTALLED WHILE PERFORMING MAINTENANCE HAD NOT BEEN | | REMOVED AS REQUIRED. | | | | THE FOLLOWING TEXT IS A PORTION OF A FACSIMILE RECEIVED FROM THE LICENSEE: | | | | "WHILE PERFORMING CRD TIMING, [THE] CONTROL ROD 38-15 FULL-IN LIGHT DID NOT | | EXTINGUISH WHEN [THE] ROD WAS WITHDRAWN. INVESTIGATION REVEALED THAT THE | | CONTROL ROD FULL-IN POSITION WAS BYPASSED TO INDICATE FULL IN REGARDLESS OF | | ACTUAL POSITION. [JUMPERS] HAD BEEN INSTALLED ON 09/13/98 FOR 32 CONTROL | | RODS SO THAT THEY COULD BE WITHDRAWN TO ALLOW CONTROL ROD BLADE/DRIVE | | REPLACEMENT. FUEL HAD BEEN REMOVED FROM THESE CELLS. [THE] JUMPER SHOULD | | HAVE BEEN REMOVED ON 09/25/98 WHEN THE OTHER 31 JUMPERS WERE REMOVED. [A] | | COMPLETE INVESTIGATION IS IN PROGRESS. CONTROL ROD MOVEMENT HAS BEEN | | STOPPED." | | | | THE LICENSEE PERFORMED A REPORTABILITY ASSESSMENT WHICH CONCLUDED THAT HAD | | CONTROL ROD 38-15 AND AN ADJACENT CONTROL ROD BEEN WITHDRAWN, A LOCAL | | CRITICALITY MAY HAVE OCCURRED. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 34873 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: NORTH ANNA REGION: 2 |NOTIFICATION DATE: 10/05/98 | |UNIT: [1] [ ] [ ] STATE: VA |NOTIFICATION TIME: 14:48 [ET]| |RX TYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 10/05/98 | +------------------------------------------------+EVENT TIME: 13:35[EDT]| |NRC NOTIFIED BY: JAMES JOHNSTONE |LAST UPDATE DATE: 10/05/98 | |HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |ANN BOLAND RDO | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N N 0 COLD SHUTDOWN | 0 COLD SHUTDOWN | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE NOTIFIED STATE DEPARTMENT OF ENVIRONMENTAL QUALITY (DEQ) | | CONCERNING AN [NON]-PERMITTED BEARING COOLING WATER SYSTEM DISCHARGE PATH. | | | | THE FOLLOWING TEXT IS A PORTION OF A FACSIMILE RECEIVED FROM THE LICENSEE: | | "AT 1335 ON 10/05/98 THE VIRGINIA DEPARTMENT OF ENVIRONMENTAL QUALITY WAS | | NOTIFIED THAT AN [NON]-PERMITTED LIQUID RELEASE WAS MADE ON THIS DATE." | | | | "THE RELEASE WAS FROM THE STATION BEARING COOLING WATER SYSTEM COOLING | | TOWER. THIS IS A NON-RADIOACTIVE, NON-HAZARDOUS SYSTEM. THE REPORT TO DEQ | | WAS MADE BECAUSE THE TOWER OVERFLOWED TO THE LAKE DURING PERFORMANCE OF THE | | PROCEDURE FOR SHIFTING FROM TOWER-TO-TOWER TO LAKE-TO-LAKE AND THEN BACK TO | | TOWER-TO-TOWER. THE [BEARING COOLING] SYSTEM WAS FLOWING TO THE TOWER FROM | | THE LAKE FOR APPROXIMATELY [2] MINUTES DURING THE EVOLUTION. THE | | COMPLETION OF THE EVOLUTION WAS DELAYED DUE TO SLUGGISH [MOTOR-OPERATED | | VALVE] AUTOMATIC OPERATION." | | | | THE LICENSEE PLANS TO INFORM THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 34874 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: SEABROOK REGION: 1 |NOTIFICATION DATE: 10/05/98 | |UNIT: [1] [ ] [ ] STATE: NH |NOTIFICATION TIME: 17:40 [ET]| |RX TYPE: [1] W-4-LP |EVENT DATE: 10/05/98 | +------------------------------------------------+EVENT TIME: 17:00[EDT]| |NRC NOTIFIED BY: MICHAEL DAVID |LAST UPDATE DATE: 10/05/98 | |HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |JAMES LINVILLE RDO | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE FOUND A DEAD SEAL ADJACENT TO THE CIRCULATING WATER INLET | | SCREEN. | | | | THE FOLLOWING TEXT IS A PORTION OF A FACSIMILE RECEIVED FROM THE LICENSEE: | | | | "A DEAD SEAL HAS BEEN FOUND ADJACENT TO THE CIRCULATING WATER INLET SCREEN. | | THIS OCCURRENCE IS REPORTABLE PER APPENDIX 'B' TO FACILITY OPERATING | | LICENSE NO. NPF-86 FOR SEABROOK STATION (NON-RADIOLOGICAL ENVIRONMENTAL | | PROTECTION PLAN) PARAGRAPH 4.1 AS A 24-HOUR REPORT." | | | | "THE NATIONAL MARINE FISHERIES WILL BE CONTACTED ON 10/06/98." | | | | THE LICENSEE INFORMED STATE/LOCAL AGENCIES AND THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 34875 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 10/05/98 | |UNIT: [1] [2] [ ] STATE: IL |NOTIFICATION TIME: 17:42 [ET]| |RX TYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 10/05/98 | +------------------------------------------------+EVENT TIME: 15:58[CDT]| |NRC NOTIFIED BY: JOHN HOPMAN |LAST UPDATE DATE: 10/05/98 | |HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: UNUSUAL EVENT +-----------------------------+ |10 CFR SECTION: |THOMAS KOZAK RDO | |AAEC 50.72(a)(1)(i) EMERGENCY DECLARED |JOHN ZWOLINSKI, NRR EO | | |CHUCK DEPUY FEMA | | |JOSEPH GIITTER, AEOD IRD | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | 2 | N N 0 REFUELING | 0 REFUELING | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE DECLARED AN UNUSUAL EVENT DUE TO MEDICAL TRANSPORT OF A | | CONTAMINATED DIVER TO A LOCAL HOSPITAL. | | | | "AT 1558 CDT, THE SITE ENTERED A GSEP UNUSUAL EVENT (EAL HU7), | | 'TRANSPORTATION OF A RADIOACTIVELY CONTAMINATED PERSON TO AN OFFSITE | | MEDICAL FACILITY.' A DIVER WAS IN THE UNIT 2 SUPPRESSION POOL AND LOST | | CONSCIOUSNESS. HE HAS BEEN EXTRACTED AND WAS RESUSCITATED AND IS ENROUTE | | TO ST. MARY'S HOSPITAL IN STREATOR, IL. IT WAS CONFIRMED HIS FACE IS | | CONTAMINATED, AND HE IS BEING ACCOMPANIED BY RADIATION PROTECTION | | PERSONNEL." | | | | THE LICENSEE DOES NOT PLAN TO ISSUE A PRESS RELEASE AT THIS TIME AND HAS | | INFORMED STATE/LOCAL AGENCIES AND THE NRC RESIDENT INSPECTOR. | | | | * * * UPDATE AT 2009 EDT ON 10/05/98 FROM JOHN HOPMAN TO S.SANDIN * * * | | | | THE LICENSEE TERMINATED THE UNUSUAL EVENT AT 1845 CDT. THE DIVER HAS BEEN | | DECONTAMINATED (BETWEEN 2-5K DPM TO THE HAIR) AND WILL BE KEPT IN THE | | HOSPITAL OVERNIGHT FOR OBSERVATION. AN INVESTIGATION WILL BE PERFORMED TO | | DETERMINE THE ROOT CAUSE. | | | | THE LICENSEE NOTIFIED STATE/LOCAL AGENCIES AND THE NRC RESIDENT INSPECTOR. | | THE NRC RESIDENT INSPECTOR NOTIFIED THE R3DO (KOZAK), NRR EO (ZWOLINSKI), | | AND FEMA (DEPUY). | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 34876 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: COOPER REGION: 4 |NOTIFICATION DATE: 10/05/98 | |UNIT: [1] [ ] [ ] STATE: NE |NOTIFICATION TIME: 18:31 [ET]| |RX TYPE: [1] GE-4 |EVENT DATE: 10/05/98 | +------------------------------------------------+EVENT TIME: 14:44[CDT]| |NRC NOTIFIED BY: JOHN OSWALD |LAST UPDATE DATE: 10/05/98 | |HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |TOM STETKA RDO | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | A N 0 REFUELING | 0 REFUELING | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE UNIT EXPERIENCED SEVERAL REACTOR PROTECTION SYSTEM ACTUATIONS. | | | | THE FOLLOWING TEXT IS A PORTION OF A FACSIMILE RECEIVED FROM THE LICENSEE: | | | | "AT 1443 CDT, [INTERMEDIATE-RANGE MONITOR (IRM)] 'E' SPIKED HIGH AND CAUSED | | AN 'A' CHANNEL AUTOMATIC SCRAM. [THE] 'B' CHANNEL SCRAM WAS ALREADY IN DUE | | TO INOPERABLE IRMs ON CHANNEL 'B.' AT THE TIME, WORK ON [SOURCE-RANGE | | MONITORS] AND IRMs WAS IN PROGRESS, AND THE SPIKE APPEARS TO BE MAINTENANCE | | RELATED." | | | | "AT 1444 CDT, A LICENSED CONTROL ROOM OPERATOR RESET THE SCRAM MOMENTARILY | | AND ANOTHER 'A' CHANNEL AUTOMATIC SCRAM OCCURRED DUE TO SCRAM DISCHARGE | | INSTRUMENT VOLUME (SDIV) HIGH WATER LEVEL. WHEN THE FIRST SCRAM WAS RESET, | | THE SDIV HIGH WATER LEVEL TRIP WAS CLEAR. SHORTLY AFTER RESETTING THE | | FIRST SCRAM, THE SDIV TRIP OCCURRED. THE OPERATOR BYPASSED THE SDIV HIGH | | WATER LEVEL TRIP IN ACCORDANCE WITH STATION PROCEDURE, AND THE 'A' CHANNEL | | SCRAM WAS RESET AT 1445 CDT." | | | | "ALL AUTOMATIC ACTIONS OCCURRED AS EXPECTED. THE PLANT WAS, AND IS, SHUT | | DOWN IN MODE 5 FOR A REFUELING OUTAGE WITH THE VESSEL HEAD ON AND | | DETENSIONED. " | | | | THERE WAS NO CONTROL ROD MOTION. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+