U.S. Nuclear Regulatory Commission Operations Center Event Reports For 12/22/97 - 12/23/97 ** EVENT NUMBERS ** 33440 33441 33442 33443 33444 33445 33446 33447 +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 33440 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: DRESDEN REGION: 3 |NOTIFICATION DATE: 12/22/97 | |UNIT: [ ] [2] [ ] STATE: IL |NOTIFICATION TIME: 05:20 [ET]| |RX TYPE: [1] GE-1,[2] GE-3,[3] GE-3 |EVENT DATE: 12/22/97 | +------------------------------------------------+EVENT TIME: 03:03[CST]| |NRC NOTIFIED BY: KEITH POLSON |LAST UPDATE DATE: 12/22/97 | |HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |BRUCE JORGENSEN RDO | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | 2 | N Y 99 POWER OPERATION | 99 POWER OPERATION | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ESF ACTUATION - HPCI ISOLATION DURING A ROUTINE SURVEILLANCE | | | | HPCI ISOLATED FOR UNKNOWN REASONS DURING THE PERFORMANCE OF THE HPCI LOW | | PRESSURE ISOLATION CHANNEL FUNCTIONAL TEST. INSTEAD OF RECEIVING THE | | EXPECTED HALF ISOLATION SIGNAL, A FULL ISOLATION SIGNAL WAS RECEIVED. THE | | HPCI SYSTEM HAS BEEN DECLARED INOPERABLE. A ROOT CAUSE INVESTIGATION HAS | | BEEN INITIATED. ALL OTHER SAFETY RELATED EQUIPMENT IS OPERABLE. | | | | THE NRC RESIDENT INSPECTOR WILL BE NOTIFIED. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |TRANSPORTATION EVENT | |EVENT NUMBER: 33441 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |LICENSEE: UNKNOWN |NOTIFICATION DATE: 12/22/97 | | CITY: REGION: 4 |NOTIFICATION TIME: 07:00 [ET]| | COUNTY: FAYETTE STATE: TX |EVENT DATE: 12/22/97 | |LICENSE#: AGREEMENT: Y |EVENT TIME: 04:30[CST]| | DOCKET: |LAST UPDATE DATE: 12/22/97 | | +-----------------------------+ | |PERSON ORGANIZATION| | |GARY SANBORN RDO | | |SUSAN SHANKMAN EO | +------------------------------------------------+RICH BARRETT IRD | |NRC NOTIFIED BY: NAT'L RESPONSE CENTER |GENE BATES RIV | |HQ OPS OFFICER: DOUG WEAVER |JOHN COOK NMSS | +------------------------------------------------+ | |EMERGENCY CLASS: NOT APPLICABLE | | |10 CFR SECTION: | | |NTRA TRANSPORTATION EVENT | | | | | | | | | | | | | | +------------------------------------------------+-----------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ACCIDENT INVOLVING TWO TRACTOR TRAILERS | | | | THIS EVENT WAS REPORTED TO THE OPERATIONS CENTER BY THE NATIONAL RESPONSE | | CENTER. | | | | A ROADWAY EXPRESS TRUCK CONTAINING RADIOACTIVE MATERIAL WAS INVOLVED IN AN | | ACCIDENT ON INTERSTATE 10 JUST EAST OF ITS INTERSECTION WITH HWY 77 IN THE | | WEST BOUND LANES. THE RADIOACTIVE MATERIAL CONTAINERS FELL ON TO THE ROAD, | | BUT NO RELEASE OF RADIOACTIVITY WAS NOTED. THE TYPE AND AMOUNT OF | | RADIOACTIVE MATERIAL WAS NOT REPORTED. THE NATIONAL RESPONSE CENTER | | NOTIFIED THE STATE OF TEXAS OF THIS EVENT. | | | | ***UPDATE ON 12/22/97 @ 1338 EST BY LINDA HOWELL (NRC REGION 4) TAKEN BY | | MACKINNON*** | | | | ALL THE FOLLOWING INFORMATION IS THIRD HAND INFORMATION RELAYED TO NRC | | REGION 4: | | | | THE PACKAGES CONTAINED 4 OHMART GAUGES (PROBABLY USED FOR PROCESS LINES). | | OHMART IS AN NRC LICENSEE LOCATED IN NRC REGION 3. THE MODEL NUMBER OF THE | | GAUGES IS A-2102 AND EACH GAUGE CONTAINS A 120 mCi CS-137 SOURCE. EACH | | GAUGE WAS PACKED IN A TRANSPORT CONTAINER AND PLACED IN A WOODEN OVERPACK. | | WHEN THE TWO TRUCKS COLLIDED IT WAS THE WOODEN OVERPACK THAT WAS THROWN | | OVER THE TRAILER AND BASICALLY DESTROYED. THE TRANSPORT CONTAINERS FOR THE | | GAUGES LOOKED "OK" AND ROADWAY'S RADIATION CONTRACTOR, ENVIRONMENTAL | | SERVICES COMPANY OF SAN ANTONIO, PERFORMED THE RADIATION SURVEYS. | | ENVIRONMENTAL SERVICES COMPANY PERSONNEL WENT TO THE SCENE OF THE ACCIDENT | | AND TOOK RADIATION SURVEYS. LINDA SAID THAT SHE DID NOT HAVE ANY OF THE | | RADIATION SURVEY VALUES BUT ENVIRONMENTAL SERVICES COMPANY SAID THEY HAD | | SURVEYED THE AREA OF THE ACCIDENT AND FOUND NO CONTAMINATION OR UNUSUAL | | RADIATION LEVELS ON THE TRANSPORT CONTAINERS. | | | | THE ORIGINAL SHIPPING PAPERS FOR THE CONTAINERS IDENTIFIED A TRANSPORT | | INDEX OF 0.1 (MEANS A RADIATION READING OF 0.1 mRem/hr AT 3 FEET). ROADWAY | | IS REPORTED TO HAVE CONTACTED OHMART AND TO HAVE A MANAGER GO ON SITE FROM | | A LOCAL ROADWAY OFFICE. OHMART AND ROADWAY DECIDED TO TAKE THE GAUGES TO | | THE NEXT CLOSEST TOWN. ROADWAY WILL STORE THE CONTAINERS HOLDING THE GAUGES | | UNTIL THEY CAN GET ANOTHER WOODEN OVERPACK AND THEN RESUME SHIPPING THE | | GAUGES TO MEXICO. | | | | NRC REGION 4 CONTACTED NRC REGION 3 OFFICE AND NOTIFIED THEM OF THIS EVENT. | | NRC REGION 4 WANTS NRC REGION 3 TO VERIFY WITH OHMART THAT THEY HAVE A | | LEVEL OF CONFIDENCE THAT THESE GAUGES WERE NOT DAMAGED OR THAT THE SHUTTERS | | ON THE GAUGES DID NOT COME OPEN DUE TO THE IMPACT OF THE ACCIDENT. | | R4DO (IAN BARNES), IRD MGR (RICH BARRETT), & NMSS EO (DON COOL) NOTIFIED. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |GENERAL INFORMATION or OTHER | |EVENT NUMBER: 33442 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |LICENSEE: ROCHESTER GAS & ELECTRIC CORP |NOTIFICATION DATE: 12/22/97 | | CITY: ROCHESTER REGION: 1 |NOTIFICATION TIME: 09:10 [ET]| | COUNTY: STATE: NY |EVENT DATE: 11/14/97 | |LICENSE#: AGREEMENT: Y |EVENT TIME: 12:00[EST]| | DOCKET: |LAST UPDATE DATE: 12/22/97 | | +-----------------------------+ | |PERSON ORGANIZATION| | |JAMES NOGGLE RDO | | | | +------------------------------------------------+JERRY CARTER NRR | |NRC NOTIFIED BY: JOHN ST. MARTEN | | |HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: NOT APPLICABLE | | |10 CFR SECTION: | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------+-----------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PART 21 - DEFECTIVE SHUNT TRIP COILS | | | | THE LICENSEE DISCOVERED A WESTINGHOUSE DB-75 BREAKER THAT WAS FAILING TO | | CLOSE AT THEIR GINNA PLANT. THE PLUNGER OF THE SHUNT TRIP COIL ASSEMBLY | | WAS BINDING, MAINTAINING THE BREAKER TRIPPER BAR IN THE TRIP FREE POSITION. | | THE LICENSEE HAS SEVEN DB-75 BREAKERS ON SITE, ONLY ONE HAD THE PROBLEM | | DESCRIBED. THE BREAKER WITH THE FAILED SHUNT TRIP COIL IS THE ONLY ONE TO | | HAVE HAD THAT PART PREVIOUSLY REPLACED. THE REPLACEMENT SHUNT TRIP COIL | | THAT FAILED WAS ONE OF TEN PURCHASED IN 1977 AS SPARES. | | | | THE FAILED SHUNT TRIP COIL WAS REPLACED WITH A SPARE FROM STOCK. THE | | REMAINING EIGHT ASSEMBLIES IN STOCK WERE INSPECTED. TWO ASSEMBLIES HAD | | COIL PLUNGERS THAT DID NOT FULLY RETURN TO THE DEENERGIZED POSITION DURING | | MANUAL MANIPULATION. THESE WERE REMOVED FROM STOCK. | | | | LICENSEE RECOMMENDS RECEIPT INSPECTION TO VERIFY ACCEPTABLE PLUNGER | | MOVEMENT AND ALSO VERIFYING THAT THE SHUNT TRIP COIL PLUNGER MOVES FREELY | | IN THE COIL ASSEMBLY DURING BREAKER MAINTENANCE. | | | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 33443 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: MILLSTONE REGION: 1 |NOTIFICATION DATE: 12/22/97 | |UNIT: [ ] [ ] [3] STATE: CT |NOTIFICATION TIME: 11:36 [ET]| |RX TYPE: [1] GE-3,[2] CE,[3] W-4-LP |EVENT DATE: 12/22/97 | +------------------------------------------------+EVENT TIME: 10:30[EST]| |NRC NOTIFIED BY: COVIN |LAST UPDATE DATE: 12/22/97 | |HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |DAN HOLODY RDO | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | | | | 3 | N N 0 COLD SHUTDOWN | 0 COLD SHUTDOWN | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE NOTIFIED THE STATE DEPARTMENT OF ENVIRONMENTAL PROTECTION THAT | | THE PLANT EXCEEDED THE NATIONAL POLLUTANT DISCHARGE ELIMINATION SYSTEM | | (NPDES) PERMIT LIMIT. | | | | THE PROBLEM WAS DUE TO A CHARCOAL FILTER AT A WATER PROCESSING FACILITY | | CAUSING A HIGH pH. THE FILTER WAS ISOLATED, THE PROBLEM HAS BEEN CORRECTED | | AND THE EVENT WAS TERMINATED. THE RESIDENT INSPECTOR HAS BEEN NOTIFIED. | | | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 33444 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: LIMERICK REGION: 1 |NOTIFICATION DATE: 12/22/97 | |UNIT: [1] [ ] [ ] STATE: PA |NOTIFICATION TIME: 14:12 [ET]| |RX TYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 12/22/97 | +------------------------------------------------+EVENT TIME: 11:05[EST]| |NRC NOTIFIED BY: GREG RUPPERT |LAST UPDATE DATE: 12/22/97 | |HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |DAN HOLODY RDO | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | RESIDUAL HEAT REMOVAL SERVICE WATER PUMP TRIPPED DUE TO A SPURIOUS | | RADIATION TRIP SIGNAL. | | | | | | THE "OB" RESIDUAL HEAT REMOVAL SERVICE WATER PUMP TRIPPED DUE TO A SPURIOUS | | RADIATION TRIP GENERATED ON THE "B" RADIATION MONITOR. ALL APPLICABLE | | PROCEDURES WERE REFERENCED AND PERFORMED. ALL SYSTEMS FUNCTIONED AS | | DESIGNED. A SAMPLE WAS TAKEN BY CHEMISTRY AND IT WAS CLEAN. AT THE TIME OF | | THE TRIP, WORKERS WERE IN THE AREA OF THE SAMPLE RACK AND WELDING WAS IN | | PROGRESS. FOLLOW-UP REVEALED THAT SOME OF THE DETECTOR CABLE CONNECTORS | | WERE LOOSE CAUSING A HIGH-HIGH RADIATION LEVEL ALARM SIGNAL. THE LICENSEE | | THINKS THAT ONE OF THE WORKERS HAD BUMPED THE CABLE CAUSING THE HIGH-HIGH | | RADIATION LEVEL ALARM SIGNAL TO BE GENERATED. | | | | THE NRC RESIDENT INSPECTOR WAS NOTIFIED OF THIS EVENT BY THE LICENSEE. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |FUEL CYCLE FACILITY | |EVENT NUMBER: 33445 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 12/22/97 | | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 17:53 [ET]| |COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 12/22/97 | | 6903 ROCKLEDGE DRIVE |EVENT TIME: 17:36[EST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 12/22/97 | | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION| |LICENSE#: GDP-2 AGREEMENT: N |JIM CREED RDO | | DOCKET: 0707002 | | +------------------------------------------------+ | |NRC NOTIFIED BY: G BARCH | | |HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: NOT APPLICABLE | | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------+-----------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SAFEGUARDS INFORMATION FOUND IN PROTECTED AREA. IMMEDIATE COMPENSATORY | | ACTIONS WERE TAKEN UPON DISCOVERY. | | | | THE NRC RESIDENT INSPECTOR WAS NOTIFIED OF THIS INCIDENT BY THE LICENSEE. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 33446 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 12/22/97 | |UNIT: [1] [ ] [ ] STATE: IL |NOTIFICATION TIME: 19:25 [ET]| |RX TYPE: [1] GE-6 |EVENT DATE: 12/22/97 | +------------------------------------------------+EVENT TIME: 17:15[CST]| |NRC NOTIFIED BY: M FUNKHOUSER |LAST UPDATE DATE: 12/22/97 | |HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |BRUCE JORGENSEN RDO | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N N 0 COLD SHUTDOWN | 0 COLD SHUTDOWN | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SHUTDOWN SERVICE WATER COOLER FAN WAS FOUND TO BE MISSING A KEY THAT | | CONNECTS THE MOTOR SHAFT TO THE FAN HUB. | | | | THE DIVISION 2 SHUTDOWN SERVICE WATER COOLER FAN WAS FOUND TO BE MISSING A | | KEY THAT CONNECTS THE MOTOR SHAFT TO THE FAN HUB. THE FAN AND COIL CABINET | | IS CAPABLE OF DISSIPATING THE HEAT PRODUCED BY THE OPERATIONS OF THE | | CORRESPONDING PUMP AND MOTOR TO LIMIT THE INSIDE ROOM TEMPERATURE TO 122 | | DEGREES F. | | | | THE FAN HAS BEEN STARTED AND OPERATED WITH NO VIBRATIONAL PROBLEMS | | THROUGHOUT IT'S PLANT HISTORY. THE FAN HAS PERFORMED WELL ENOUGH TO | | MAINTAIN A DIFFERENTIAL PRESSURE ABOVE 1.2 INCHES WATER COLUMN. THE | | SUBJECTED SHUTDOWN SERVICE WATER ROOM HAS NEVER EXPERIENCED A HIGH | | TEMPERATURE ALARM. HOWEVER, THE DESIGN REQUIREMENT FOR THE FAN TO PRODUCE | | 30,000 STANDARD CUBIC FEET PER MINUTE AT 2 INCHES WATER COLUMN HAS NOT BEEN | | VERIFIED SINCE PRE-OPERATIONAL TESTING. THE LICENSEE WILL INSPECT THE | | REMAINING 480 VOLT MOTORS THAT HAVE NOT BEEN INSPECTED TO MAKE SURE THEY | | HAVE A KEY THAT CONNECTS THE MOTOR SHAFT TO THE FAN HUB. | | | | THIS CONDITION APPEARS TO HAVE EXISTED SINCE START-UP. THIS CONDITION MAY | | HAVE PLACED THE PLANT IN AN UNANALYZED CONDITION THAT SIGNIFICANTLY | | COMPROMISED PLANT SAFETY. | | | | THE NRC RESIDENT INSPECTOR WAS NOTIFIED OF THIS EVENT BY THE LICENSEE. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 33447 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 12/23/97 | |UNIT: [ ] [3] [ ] STATE: NY |NOTIFICATION TIME: 03:53 [ET]| |RX TYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 12/23/97 | +------------------------------------------------+EVENT TIME: 03:00[EST]| |NRC NOTIFIED BY: VINCENT DE CLEMENTE |LAST UPDATE DATE: 12/23/97 | |HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |DAN HOLODY RDO | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | 3 | N N 0 HOT SHUTDOWN | 0 HOT SHUTDOWN | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TECH SPEC REQUIRED SHUTDOWN AND OUTSIDE DESIGN BASIS | | | | THE LICENSEE HAS COMMENCED A COOL DOWN TO COLD SHUTDOWN BECAUSE ALL THREE | | EDGs HAVE BEEN DECLARED INOPERABLE. THE LICENSEE SUSPECTS THAT MULTIPLE | | 480 VOLT CIRCUIT BREAKERS WOULD NOT TRIP WHEN CALLED UPON TO DO SO. THIS | | COULD POTENTIALLY OVERLOAD THE EDGs SINCE SOME LOADS MIGHT NOT BE STRIPPED | | FROM THE EMERGENCY BUSES AS AS REQUIRED. TWO DEFICIENT BREAKERS HAVE BEEN | | IDENTIFIED OUT OF THE FIVE BREAKERS INSPECTED. SIXTEEN BREAKERS ARE | | SUSPECT BASED ON HAVING HAD WORK PERFORMED UPON THEM BY THE SAME | | CONTRACTOR, POWER DISTRIBUTION TECHNOLOGY. THE WORK WAS PERFORMED BETWEEN | | 1990 AND 1993. | | | | THE DEFICIENCY FOUND INVOLVES AN OVEREXTENDED MECHANICAL LINKAGE THAT | | PREVENTS THE BREAKERS FROM TRIPPING. | | | | THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR. | | | | SEE RELATED REPORT #33425. | +------------------------------------------------------------------------------+