U.S. Nuclear Regulatory Commission Operations Center Event Reports For 07/18/97 - 07/21/97 ** EVENT NUMBERS ** 32456 32644 32645 32646 32647 32648 32649 32650 32651 32652 32653 32654 32655 32656 32657 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 32456 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: VERMONT YANKEE REGION: 1 |NOTIFICATION DATE: 06/10/97 | |UNIT: [1] [ ] [ ] STATE: VT |NOTIFICATION TIME: 16:33 [ET]| |RX TYPE: [1] GE-4 |EVENT DATE: 06/10/97 | +------------------------------------------------+EVENT TIME: 16:15[EDT]| |NRC NOTIFIED BY: WISNIEWSKI |LAST UPDATE DATE: 07/18/97 | |HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |RICHARD KEIMIG RDO | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE DISCOVERED THEY HAVE NON-NUCLEAR SAFETY PRESSURE REGULATORS | | PROVIDING ALTERNATE COOLING TO THE EMERGENCY DIESEL GENERATORS(EDG's). | | | | DURING AN EQUIPMENT REVIEW BY INSTRUMENT & CONTROL PERSONNEL, IT WAS | | DISCOVERED THAT THE CONTROLLERS FOR "PCV-104-69A/B" USE NON-NUCLEAR SAFETY | | PRESSURE REGULATORS WHEN THE VALVES PERFORM A SAFETY FUNCTION (PROVIDE | | ALTERNATE COOLING TO THE EDG's). THE PRESSURE REGULATORS, HOWEVER, ARE | | CONSIDERED OPERABLE, THEREFORE ALTERNATE COOLING TO THE EDG's IS STILL | | OPERABLE. THE OPERATING PROCEDURES FOR ALTERNATE COOLING REQUIRE OPENING | | THE MANUAL ISOLATION VALVE TO THE PRESSURE CONTROL VALVE AND TO MANUALLY | | POSITIONING IT IF THE PRESSURE CONTROL VALVE IS NOT PERFORMING ITS | | FUNCTION. THEY CURRENTLY HAVE A WORK ORDER REQUEST IN TO REPLACE THESE | | REGULATORS WITH SAFETY CLASS REGULATORS. THEY ARE NOT IN ANY TYPE OF LCO | | ACTION STATEMENT. THE RESIDENT INSPECTOR HAS BEEN NOTIFIED. | | | | HOO NOTE: SEE SIMILAR EVENT #32370. | | | | * * * UPDATE AT 0958 ON 07/18/97 BY HALLONQUIST ENTERED BY WEAVER * * * | | | | THE LICENSEE IS RETRACTING THIS EVENT REPORT. LICENSEE ENGINEERING | | PERSONNEL EVALUATED THE EQUIPMENT AND FOUND IT TO BE OF THE PROPER QUALITY. | | EACH PIECE OF EQUIPMENT IS USED ELSEWHERE IN THE FACILITY IN SEISMIC | | CONFIGURATION APPLICATIONS AND THE SEISMIC CONFIGURATION WAS FOUND CAPABLE | | OF SUPPORTING EQUIPMENT SAFETY FUNCTIONS. THE LICENSEE WILL NOTIFY THE NRC | | RESIDENT INSPECTOR. THE HOO INFORMED THE R1DO (HERB WILLIAMS). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 32644 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: LIMERICK REGION: 1 |NOTIFICATION DATE: 07/17/97 | |UNIT: [1] [2] [ ] STATE: PA |NOTIFICATION TIME: 21:27 [ET]| |RX TYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 07/17/97 | +------------------------------------------------+EVENT TIME: 17:34[EDT]| |NRC NOTIFIED BY: RAY LANDIS |LAST UPDATE DATE: 07/18/97 | |HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |HERB WILLIAMS RDO | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | 2 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - GROUP 6A PCIS INITIATED FOR UNITS 1 & 2 DUE TO HI-HI RAD MONITOR SIGNAL - | | | | AT 1734, WHILE TECHNICIANS WERE PERFORMING A PURGE OF THE UNIT 1 DRYWELL, | | A GROUP 6A PRIMARY CONTAINMENT ISOLATION SIGNAL (PCIS) WAS INITIATED FOR | | UNITS 1 & 2 DUE TO ONE OF THREE NORTH VENTILATION STACK RADIATION MONITORS | | (WIDE RANGE) EXCEEDING ITS HIGH-HIGH RADIATION SIGNAL SETPOINT. NO | | CONTAINMENT PURGE SUPPLY AND EXHAUST VALVES CLOSED ON EITHER UNIT SINCE | | ALL THE GROUP 6A ISOLATION VALVES WERE ALREADY CLOSED. THERE WERE NO | | INDICATIONS OF INCREASED RADIATION LEVELS SENSED BY OTHER OPERABLE NORTH | | STACK GASEOUS RADIATION MONITORS. | | | | AT 2120, THE LICENSEE RESET ALL SYSTEMS TO NORMAL. THE LICENSEE IS | | INVESTIGATING THE CAUSE OF THIS EVENT AND SUSPECTS THAT THE WIDE RANGE | | RADIATION MONITOR IS FAULTY. | | | | THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR. | | | | * * * UPDATE AT 1545 ON 07/18/97 BY GLENN STEWART ENTERED BY JOLLIFFE * * * | | | | THE LICENSEE DETERMINED THAT THE HIGH-HIGH RADIATION SIGNAL WAS A SPURIOUS | | SIGNAL CAUSED BY AN ELECTRICAL SPIKE, AND THEREFORE, WAS AN INVALID SIGNAL. | | THIS DETERMINATION IS SUPPORTED BY THE RESULTS OF A GRAB SAMPLE ANALYSIS | | WHICH INDICATED THAT NO INCREASED RADIATION LEVELS WERE PRESENT IN THE | | NORTH VENTILATION STACK. THUS, THE LICENSEE DESIRES TO RETRACT THIS EVENT. | | | | THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR. THE OPERATIONS | | OFFICER NOTIFIED THE R1DO HERB WILLIAMS. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 32645 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: WATERFORD REGION: 4 |NOTIFICATION DATE: 07/18/97 | |UNIT: [3] [ ] [ ] STATE: LA |NOTIFICATION TIME: 03:39 [ET]| |RX TYPE: [3] CE |EVENT DATE: 07/18/97 | +------------------------------------------------+EVENT TIME: 02:20[CDT]| |NRC NOTIFIED BY: GRUBB |LAST UPDATE DATE: 07/18/97 | |HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: UNUSUAL EVENT +-----------------------------+ |10 CFR SECTION: |JOHN POTTER RDO | |AAEC 50.72(a)(1)(i) EMERGENCY DECLARED |STUART RICHARDS, NRR EO | |NOCM COMM ASST BRIEF |CALDWELL FEMA | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 3 | N N 0 HOT SHUTDOWN | 0 HOT SHUTDOWN | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT - HURRICANE WARNING FOR ST. CHARLES PARISH, LOUISIANA. | | | | THE LICENSEE DECLARED AN UNUSUAL EVENT IN ACCORDANCE WITH THEIR EMERGENCY | | PLAN WHEN A HURRICANE WARNING WAS DECLARED FOR ST. CHARLES PARISH, LA. | | HURRICANE DANNY IS PRESENTLY APPROXIMATELY 40 MILES SOUTHWEST OF | | BOOTHVILLE, LA, WITH MAXIMUM SUSTAINED WINDS OF 75 MPH AND IS MOVING VERY | | SLOWLY TO THE NORTHEAST. | | | | THE LICENSEE IS IN MODE 4 (HOT SHUTDOWN) MAKING PREPARATIONS TO GO TO | | MODE 5 (COLD SHUTDOWN). THE PLANT HAS BEEN SHUT DOWN SINCE 04/11/97. ALL | | OFFSITE POWER SOURCES AND ALL EMERGENCY DIESEL GENERATORS ARE AVAILABLE. | | | | THE LICENSEE NOTIFIED THE LOUISIANA OFFICE OF EMERGENCY PREPAREDNESS AND | | THE EMERGENCY OPERATIONS CENTERS FOR ST. CHARLES AND ST. JOHNS PARISHES. | | | | THE LICENSEE NOTIFIED THE NRC RESIDENT INSPECTOR. | | | | * * * UPDATE @ 1000 ON 07/18/97 BY WEAVER * * * | | | | A COMMISSIONERS' ASSISTANTS BRIEFING WAS HELD AT 1000 ON 07/18/97 BY REGION | | 4 BILL JONES AT THE REQUEST OF THE REGIONAL 4 ADMINISTRATOR. | | THE FOLLOWING ATTENDED THE BRIEFING: NRR (DENNIG), PA (BEECHER), | | SP (DROGGITTIS), IP (UPSHAW), SECY (HART), CHAIRMAN JACKSON (DEFINO), | | COMM DICUS (KOKAJKO), COMM DIAZ (SHAW), COMM McGAFFIGAN (BELL), | | EDO (HILTZ), RI (KELLER). | | | | * * * UPDATE @ 1743 ON 07/18/97 BY DAVE HERLOCKER ENTERED BY JOLLIFFE * * * | | | | AT 1623 (CDT) ON 07/18/97, THE LICENSEE TERMINATED THE UNUSUAL EVENT DUE | | TO THE CANCELLATION OF THE HURRICANE WARNING FOR ST. CHARLES PARISH, LA. | | MAXIMUM SUSTAINED WINDS OBSERVED ONSITE WERE APPROXIMATELY 25 MPH. THE | | PLANT EXPERIENCED NO DAMAGE. HURRICANE DANNY IS PRESENTLY IN THE GULF OF | | MEXICO APPROXIMATELY 65 MILES SSW OF MOBILE, AL. | | | | THE LICENSEE NOTIFIED STATE AND LOCAL OFFICIALS AND THE NRC RESIDENT | | INSPECTOR. | | | | THE OPERATIONS OFFICER NOTIFIED R4DO ELMO COLLINS, NRR EO STUART RICHARDS, | | AND FEMA KEN SWEETSER. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 32646 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: MCGUIRE REGION: 2 |NOTIFICATION DATE: 07/18/97 | |UNIT: [ ] [2] [ ] STATE: NC |NOTIFICATION TIME: 09:43 [ET]| |RX TYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 07/18/97 | +------------------------------------------------+EVENT TIME: 08:50[EDT]| |NRC NOTIFIED BY: SPENCER HACKNEY |LAST UPDATE DATE: 07/18/97 | |HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |JOHN POTTER RDO | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | 2 | N N 0 COLD SHUTDOWN | 0 COLD SHUTDOWN | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - 8 OF 24 ICE CONDENSER DOORS EXCEEDED TECH SPEC OPENING PRESSURE. | | | | THE LICENSEE'S INSPECTIONS RELATED TO EVENT #32615 REVEALED THAT 8 OF THE | | 24 ICE CONDENSER DOORS REQUIRED A HIGHER OPENING PRESSURE THAN ALLOWED BY | | TECH SPECS. THE ICE CONDENSER IS NOT REQUIRED TO BE OPERABLE IN MODE 5 | | (COLD SHUTDOWN). | | | | THE LICENSEE IS INVESTIGATING THE CAUSE OF THIS EVENT AND DETERMINING | | CORRECTIVE ACTIONS. | | | | THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |OTHER NUCLEAR MATERIAL | |EVENT NUMBER: 32647 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |LICENSEE: MISSOURI DEPT OF TRANSPORTATION |NOTIFICATION DATE: 07/18/97 | | CITY: ST LOUIS REGION: 3 |NOTIFICATION TIME: 10:00 [ET]| | COUNTY: ST LOUIS STATE: MO |EVENT DATE: 07/17/97 | |LICENSE#: 24-20415-01 AGREEMENT: N |EVENT TIME: 13:00[CDT]| | DOCKET: |LAST UPDATE DATE: 07/18/97 | | +-----------------------------+ | |PERSON ORGANIZATION| | |JOHN MADERA RDO | | |FRED COMBS, NMSS EO | +------------------------------------------------+ | |NRC NOTIFIED BY: JERRY HIRTZ | | |HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: NOT APPLICABLE | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------+-----------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | A MISSOURI DEPARTMENT OF TRANSPORTATION PICKUP TRUCK CARRYING A TROXLER | | ASPHALT CONTENT GAUGE WAS INVOLVED IN A CHAIN REACTION TRAFFIC ACCIDENT. | | THE SOURCE INSIDE THE GAUGE WAS NOT DAMAGED. | | | | A MISSOURI DEPARTMENT OF TRANSPORTATION PICKUP TRUCK CARRYING A TROXLER | | ASPHALT CONTENT GAUGE CONTAINING A 100 mCi AMERICIUM-241 SOURCE WAS | | INVOLVED IN A CHAIN REACTION TRAFFIC ACCIDENT ON I-270 NORTH OF DORSETT | | ROAD, WEST OF ST LOUIS, MO. THE GAUGE WAS CHAINED DOWN IN THE BACK OF THE | | TRUCK. THE FORCE OF THE ACCIDENT CAUSED THE CHAIN HOLDING THE GAUGE TO THE | | TRUCK TO PULL THE HANDLE OFF OF THE GAUGE. THERE WAS NO DAMAGE TO THE | | SOURCE INSIDE THE GAUGE. ONE LANE OF I-270 WAS SHUT DOWN FOR 30 TO 40 | | MINUTES TO PERFORM RADIATION SURVEYS (LEAK TEST & SWIPES TAKEN) ON THE | | TROXLER GAUGE TO INSURE THAT THERE WAS NO DAMAGE TO THE GAUGE. THE GAUGE | | WAS TAKEN TO THE MISSOURI MATERIAL LAB FOR REPAIRS. IF THE GAUGE CANNOT BE | | REPAIRED, IT WILL BE SHIPPED TO TROXLER. | | | | TROXLER ASPHALT CONTENT GAUGE INFORMATION: MODEL #3241, SERIAL #986, SOURCE | | #558331. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 32648 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 07/18/97 | |UNIT: [1] [ ] [ ] STATE: IL |NOTIFICATION TIME: 16:55 [ET]| |RX TYPE: [1] GE-6 |EVENT DATE: 07/18/97 | +------------------------------------------------+EVENT TIME: 12:00[CDT]| |NRC NOTIFIED BY: RAY DANIEL, ELGAR CORP. |LAST UPDATE DATE: 07/18/97 | |HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |JOHN MADERA RDO | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | |VERN HODGE NRR | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N N 0 COLD SHUTDOWN | 0 COLD SHUTDOWN | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | -POSSIBLE 10CFR21 REPORTABLE CONDITION RE POTENTIAL DEGRADATION OF RPS UPS- | | | | GENERAL ELECTRIC SPECIFICATION #22A3153, REVISION 5, PARAGRAPH 4.3.5.6.3 | | REQUIRES THAT POWER BEING SUPPLIED BY REACTOR PROTECTION SYSTEM (RPS) | | UNINTERRUPTIBLE POWER SUPPLY (UPS) #103-1-189 BE DISCONNECTED IF AN | | ABNORMAL VOLTAGE OR FREQUENCY CONDITION EXISTS FOR A DURATION OF 4 SECONDS | | OR MORE. | | | | AN ENGINEERING INVESTIGATION CONDUCTED BY ELGAR CORPORATION, SAN DIEGO, CA, | | AT CLINTON'S REQUEST, DETERMINED THAT WHILE THE UNDER/OVER-FREQUENCY | | CIRCUIT CAN BE CALIBRATED TO MEET THE 4 SECOND DELAY THRESHOLD, THE | | UNDER/OVER-VOLTAGE DETECTION CIRCUIT CANNOT MEET THIS SPECIFICATION DUE TO | | THE R-C TIME CONSTANT OF THE OVER-VOLTAGE CIRCUIT INPUT FILTER COMPONENTS, | | WHICH BY THEMSELVES, EXCEED THE 4 SECOND THRESHOLD AT CLINTON. | | | | ELGAR CORPORATION RECOMMENDS THAT CLINTON EVALUATE THE TIMING DELAY | | REQUIREMENTS APPLICABLE TO THE REACTOR PROTECTION SYSTEM TO DETERMINE IF | | ACTUAL PERFORMANCE IS DEGRADED AND THAT CLINTON TAKE ACTION AS APPROPRIATE. | | ELGAR CORPORATION IS PREPARED TO ASSIST IN THIS EFFORT AT CLINTON'S | | REQUEST. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 32649 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 07/18/97 | |UNIT: [1] [ ] [ ] STATE: MA |NOTIFICATION TIME: 18:45 [ET]| |RX TYPE: [1] GE-3 |EVENT DATE: 07/18/97 | +------------------------------------------------+EVENT TIME: 18:00[EDT]| |NRC NOTIFIED BY: MIKE JACOBS |LAST UPDATE DATE: 07/18/97 | |HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |HERB WILLIAMS RDO | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - SALT SERVICE WATER SYSTEM SINGLE FAILURE OUTSIDE PLANT DESIGN BASIS - | | | | THE SAFETY RELATED PLANT SALT SERVICE WATER SYSTEM (ULTIMATE HEAT SINK) | | CONSISTS OF FIVE PUMPS WHICH DISCHARGE TO A COMMON HEADER THAT SUPPLIES | | COOLING WATER FOR TWO INDEPENDENT REACTOR BUILDING CLOSED COOLING WATER | | SYSTEM LOOPS. TWO VALVES ARE PROVIDED IN THE COMMON HEADER TO ALLOW FOR | | REDUNDANT AND INDEPENDENT LOOPS FOLLOWING AN ACCIDENT. | | | | DURING A REGION I INSPECTION OF PILGRIM, THE LICENSEE IDENTIFIED A SINGLE | | FAILURE OF THIS SYSTEM THAT PLACES THE PLANT OUTSIDE ITS DESIGN BASIS. THIS | | FAILURE WOULD RESULT IN A FAILURE TO ISOLATE BOTH SALT SERVICE WATER SYSTEM | | LOOPS WHICH COULD RESULT IN A SINGLE SALT SERVICE WATER PUMP OPERATING IN A | | RUNOUT CONDITION (POTENTIAL CAVITATION). | | | | THE DESIGN BASIS (POST ACCIDENT) ASSUMES THAT ONE PUMP IN EACH LOOP IS | | RUNNING AND THAT EACH LOOP IS ISOLATED FROM EACH OTHER SUBSEQUENT TO A | | DESIGN BASIS ACCIDENT COINCIDENT WITH A LOSS OF OFFSITE POWER. | | | | THE LICENSEE HAS PERFORMED AN OPERABILITY EVALUATION AND CONSIDERS | | THE SYSTEM OPERABLE. THE LICENSEE IS IMPLEMENTING A TEMPORARY PLANT | | MODIFICATION WHICH WILL CLOSE ONE NORMALLY OPEN HEADER ISOLATION VALVE. | | THIS WILL RESTORE CONFORMANCE WITH THE PLANT DESIGN BASIS. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 32650 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 07/18/97 | |UNIT: [1] [ ] [ ] STATE: MA |NOTIFICATION TIME: 18:55 [ET]| |RX TYPE: [1] GE-3 |EVENT DATE: 07/18/97 | +------------------------------------------------+EVENT TIME: 18:00[EDT]| |NRC NOTIFIED BY: MIKE JACOBS |LAST UPDATE DATE: 07/18/97 | |HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |HERB WILLIAMS RDO | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - RHR SYSTEM FLOW RATE IN OPERATING PROCEDURE DIFFERENT THAN DBA ANALYSIS - | | | | DURING A REGION I INSPECTION OF PILGRIM, THE LICENSEE DISCOVERED THAT | | THE PLANT OPERATING PROCEDURE FOR THE RESIDUAL HEAT REMOVAL (RHR) SYSTEM | | SPECIFIES OPERATION IN THE EMERGENCY MODE THAT IS DIFFERENT THAN | | ASSUMPTIONS MADE IN THE DESIGN BASIS ACCIDENT (DBA) ANALYSIS. | | | | THE ASSUMED FLOW RATE FOR THE CONTAINMENT HEAT REMOVAL FUNCTION OF THE | | RHR SYSTEM IN THE DBA ANALYSIS IS 5100 GPM. THE RHR SYSTEM PLANT OPERATING | | PROCEDURE SPECIFIES A RANGE OF 4800 TO 5100 GPM WHEN PERFORMING THE | | CONTAINMENT HEAT REMOVAL FUNCTION. OPERATION AT THE LOWER END OF THIS | | RANGE, COUPLED WITH INSTRUMENT INACCURACIES, WOULD RESULT IN LESS HEAT | | TRANSFER THAN ASSUMED IN THE DBA ANALYSIS. | | | | THE LICENSEE HAS PERFORMED AN OPERABILITY EVALUATION AND CONSIDERS THE | | SYSTEM OPERABLE. THE LICENSEE IS IMPLEMENTING A PROCEDURE CHANGE TO ALLOW | | OPERATION UP TO 5600 GPM TO ENSURE RATED HEAT REMOVAL DURING A DBA. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 32651 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: ZION REGION: 3 |NOTIFICATION DATE: 07/19/97 | |UNIT: [1] [2] [ ] STATE: IL |NOTIFICATION TIME: 03:51 [ET]| |RX TYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 07/19/97 | +------------------------------------------------+EVENT TIME: 01:25[CDT]| |NRC NOTIFIED BY: HANSON |LAST UPDATE DATE: 07/19/97 | |HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |JOHN MADERA RDO | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N N 0 REFUELING | 0 REFUELING | | 2 | N N 0 COLD SHUTDOWN | 0 COLD SHUTDOWN | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SECURITY EVENT. SAFEGUARDS SYSTEM DEGRADATION RELATED TO PROTECTED AREA | | BOUNDARY DETECTION. IMMEDIATE COMPENSATORY MEASURES TAKEN UPON DISCOVERY. | | THE LICENSEE NOTIFIED THE NRC RESIDENT INSPECTOR. REFER TO HOO LOG FOR | | ADDITIONAL DETAILS. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |HOSPITAL | |EVENT NUMBER: 32652 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |LICENSEE: LOWER BUCKS HOSPITAL, BRISTOL, PA |NOTIFICATION DATE: 07/19/97 | | CITY: BRISTOL REGION: 1 |NOTIFICATION TIME: 12:27 [ET]| | COUNTY: STATE: PA |EVENT DATE: 07/19/97 | |LICENSE#: AGREEMENT: N |EVENT TIME: 10:00[EDT]| | DOCKET: |LAST UPDATE DATE: 07/19/97 | | +-----------------------------+ | |PERSON ORGANIZATION| | |HERB WILLIAMS RDO | | |MARGARET FEDERLINE EO | +------------------------------------------------+ | |NRC NOTIFIED BY: DR. MARK ANSLEY, RSO | | |HQ OPS OFFICER: DICK JOLLIFFE | | +------------------------------------------------+ | |EMERGENCY CLASS: NOT APPLICABLE | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------+-----------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | -HOSPITAL REMOVED UNDAMAGED PLUTONIUM CARDIAC PACEMAKER FROM DEAD PATIENT- | | | | AN UNDAMAGED PLUTONIUM CARDIAC PACEMAKER WAS REMOVED FROM A DECEASED MALE | | PATIENT AT LOWER BUCKS HOSPITAL, BRISTOL, PENNSYLVANIA. THE PACEMAKER WILL | | BE RETURNED TO ITS MANUFACTURER, BIOCONTROL COMPANY. | | | | DR. MARK ANSLEY, LOWER BUCKS HOSPITAL RADIATION SAFETY OFFICER, PLANS TO | | SUBMIT A WRITTEN REPORT TO THE NRC WITHIN 30 DAYS. | | | | REFER TO THE HOO LOG FOR DR. BUCKS' TELEPHONE NUMBERS. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 32653 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: CALLAWAY REGION: 4 |NOTIFICATION DATE: 07/19/97 | |UNIT: [1] [ ] [ ] STATE: MO |NOTIFICATION TIME: 23:34 [ET]| |RX TYPE: [1] W-4-LP |EVENT DATE: 07/19/97 | +------------------------------------------------+EVENT TIME: 16:15[CDT]| |NRC NOTIFIED BY: RON AFFOLTER |LAST UPDATE DATE: 07/19/97 | |HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: UNUSUAL EVENT +-----------------------------+ |10 CFR SECTION: |ELMO COLLINS RDO | |AAEC 50.72(a)(1)(i) EMERGENCY DECLARED |STUART RICHARDS, NRR EO | | |STINEDURF FEMA | | |JOSEPH GIITTER IRD | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 95 POWER OPERATION | 95 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | -RETROACTIVE UE DUE TO LOSS OF MOST CONTROL ROOM ANNUNCIATORS >15 MINUTES- | | | | AT 1600 (CDT), THE PLANT EXPERIENCED A LIGHTNING STRIKE THAT CAUSED THE | | FAILURE OF FOUR COMPUTER CONNECTING CARDS IN THE FIELD POWER SUPPLIES FOR | | THE CONTROL ROOM ANNUNCIATORS. THESE FOUR FAILED CONNECTING CARDS CAUSED | | THE VOLTAGE OF THE FOUR FIELD POWER SUPPLIES TO DROP FROM A NORMAL VOLTAGE | | OF 130 VOLTS TO 25 VOLTS WHICH CAUSED THE LOSS OF APPROXIMATELY 80% OF THE | | CONTROL ROOM ANNUNCIATORS. | | | | AT 1630 (CDT), TECHNICIANS DEENERGIZED THE FOUR FAILED CARDS WHICH CAUSED | | THE VOLTAGE OF THE FOUR FIELD POWER SUPPLIES TO RETURN TO 130 VOLTS. | | APPROXIMATELY 90% OF THE CONTROL ROOM ANNUNCIATORS RETURNED TO NORMAL. | | | | AT 2234 (CDT), THE LICENSEE REPORTED THAT IN ACCORDANCE WITH PLANT | | EMERGENCY ACTION LEVELS GROUP 4, CALLAWAY SHOULD HAVE BEEN PLACED IN AN | | UNUSUAL EVENT FROM 1615 TO 1630 (CDT) DUE TO AN UNPLANNED LOSS OF MOST | | CONTROL ROOM ANNUNCIATORS FOR LONGER THAN 15 MINUTES. THE INDICATOR FOR | | THIS REPORT IS THREE OF FOUR FIELD POWER SUPPLIES FAILED FOR LONGER THAN | | 15 MINUTES. ALTHOUGH THE POWER SUPPLIES HAVE NOT FAILED, DURING THE | | 30 MINUTES FROM 1600 TO 1630 (CDT), THE LICENSEE COULD NOT BE POSITIVE | | THAT THE MAJORITY OF THE ANNUNCIATORS WERE FUNCTIONAL. | | | | THE LICENSEE IS CURRENTLY REPAIRING THE FAILED CONNECTOR CARDS THAT HAVE | | APPROXIMATELY 10% OF THE CONTROL ROOM ANNUNCIATORS NOT FUNCTIONAL. THE | | PLANT EXPERIENCED NO OTHER DAMAGE AND IS STABLE AT 95% POWER. | | | | THE LICENSEE WILL NOTIFY STATE & LOCAL OFFICIALS AND THE RESIDENT INSPECTOR | | OF THE RETROACTIVE DECLARATION AND TERMINATION OF THE UNUSUAL EVENT. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 32654 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: GINNA REGION: 1 |NOTIFICATION DATE: 07/20/97 | |UNIT: [1] [ ] [ ] STATE: NY |NOTIFICATION TIME: 03:17 [ET]| |RX TYPE: [1] W-2-LP |EVENT DATE: 07/20/97 | +------------------------------------------------+EVENT TIME: 00:43[EDT]| |NRC NOTIFIED BY: DOUG GOMEZ |LAST UPDATE DATE: 07/20/97 | |HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |HERB WILLIAMS RDO | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PARTIAL LOSS OF OFFSITE POWER AND AUTO START AND LOAD OF EDG. | | | | AT 0043, OFFSITE POWER CIRCUIT #751 DEENERGIZED FOR UNKNOWN REASONS CAUSING | | A LOSS OF OFFSITE POWER TO THE #12A TRANSFORMER AND SAFEGUARDS BUSES | | #16 AND #17. EMERGENCY DIESEL GENERATOR 'B' AUTOMATICALLY STARTED AND | | LOADED TO SAFEGUARDS BUSES #16 AND #17. THE LICENSEE ENTERED PROCEDURES | | "AP ELECT.1" AND "ER ELECT.1" TO STABILIZE AND RESTORE THE PLANT ELECTRICAL | | LINEUP TO NORMAL. | | | | AT 0114, THE LICENSEE RESTORED OFFSITE POWER TO SAFEGUARDS BUSES #16 AND | | #17 VIA CIRCUIT #767 AND EDG 'B' TO STANDBY MODE. | | | | THE LICENSEE IS INVESTIGATING THE CAUSE AND DETERMINING CORRECTIVE ACTIONS. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 32655 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: HARRIS REGION: 2 |NOTIFICATION DATE: 07/20/97 | |UNIT: [1] [ ] [ ] STATE: NC |NOTIFICATION TIME: 05:27 [ET]| |RX TYPE: [1] W-3-LP |EVENT DATE: 07/20/97 | +------------------------------------------------+EVENT TIME: 02:56[EDT]| |NRC NOTIFIED BY: MARK PALMER |LAST UPDATE DATE: 07/20/97 | |HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |JOHN POTTER RDO | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | A/R Y 100 POWER OPERATION | 0 HOT STANDBY | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTO REACTOR TRIP FROM 100% POWER DUE TO FAULT IN MAIN GENERATOR EXCITER. | | | | AN AUTOMATIC TURBINE TRIP/REACTOR TRIP FROM 100% POWER OCCURRED DUE TO A | | LOSS OF GENERATOR EXCITATION CAUSED BY AN ELECTRICAL FAULT IN THE EXCITER. | | ALL CONTROL RODS INSERTED COMPLETELY AND ALL SYSTEMS FUNCTIONED AS | | EXPECTED. THE AUXILIARY FEEDWATER SYSTEM AUTOMATICALLY STARTED DUE TO LOW | | STEAM GENERATOR LEVELS FOLLOWING THE TRIP. | | | | THE PLANT IS STABLE IN MODE 3 (HOT STANDBY). | | | | THE LICENSEE HAS FOUND THREE BLOWN FUSES IN THE EXCITER AND PLANS TO | | TROUBLESHOOT AND REPAIR THE CAUSE OF THE FAULT. | | | | THE NRC RESIDENT INSPECTOR HAS BEEN INFORMED BY THE LICENSEE. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 32656 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: SEABROOK REGION: 1 |NOTIFICATION DATE: 07/20/97 | |UNIT: [1] [ ] [ ] STATE: NH |NOTIFICATION TIME: 14:15 [ET]| |RX TYPE: [1] W-4-LP |EVENT DATE: 07/20/97 | +------------------------------------------------+EVENT TIME: 05:30[EDT]| |NRC NOTIFIED BY: MARK SKETCHLEY |LAST UPDATE DATE: 07/20/97 | |HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |HERB WILLIAMS RDO | |NLTR LICENSEE 24 HR REPORT | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - DEAD SEAL WAS WASHED OFF THE PLANT CIRC WATER TRAVELING SCREEN - | | | | IN ACCORDANCE WITH SECTION 4.1 OF THE PLANT ENVIRONMENTAL PROTECTION PLAN, | | TECH SPEC APPENDIX B, THE LICENSEE IS NOTIFYING THE NRC THAT A DEAD SEAL | | WAS WASHED OFF THE PLANT CIRCULATING WATER TRAVELING SCREEN. | | | | THE LICENSEE ALSO PLANS TO NOTIFY THE NATIONAL MARINE FISHERIES SERVICE IN | | GLOUCESTER, MASSACHUSETTS. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 32657 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: SALEM REGION: 1 |NOTIFICATION DATE: 07/20/97 | |UNIT: [1] [2] [ ] STATE: NJ |NOTIFICATION TIME: 20:49 [ET]| |RX TYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 07/20/97 | +------------------------------------------------+EVENT TIME: 17:00[EDT]| |NRC NOTIFIED BY: JOHN KONOVALCHICK |LAST UPDATE DATE: 07/20/97 | |HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |HERB WILLIAMS RDO | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | |NLCO TECH SPEC LCO A/S | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N N 0 HOT STANDBY | 0 HOT STANDBY | | 2 | N N 0 REFUELING | 0 REFUELING | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - CONTROL ROOM VENTILATION SYSTEM OPERATED IN AN UNANALYZED CONDITION - | | | | SALEM UNIT 1 (MODE 6 - DEFUELED IN A REFUELING OUTAGE) AND UNIT 2 (MODE 3 - | | HOT STANDBY IN A REFUELING OUTAGE) HAVE A COMMON CONTROL ROOM. | | | | AT 1409, A MOMENTARY SPIKE OCCURRED ON THE #1B VITAL INSTRUMENT BUS DURING | | A MAINTENANCE ACTIVITY. THIS SPIKE CAUSED THE COMMON CONTROL ROOM | | VENTILATION SYSTEM TO AUTOMATICALLY SHIFT FROM THE NORMAL MODE TO THE | | ACCIDENT PRESSURIZATION MODE OF OPERATION DUE TO THE MOMENTARY LOSS OF | | POWER TO CONTROL ROOM RADIATION MONITORS #1R1B-1 (UNIT 1) AND #1R1B-2 | | (UNIT 2). | | | | AT 1700, THE LICENSEE DETERMINED THAT THE CONTROL ROOM VENTILATION SYSTEM | | WAS OPERATING IN AN UNANALYZED CONDITION SINCE THE ACCIDENT PRESSURIZATION | | OPERATING MODE OF THE CONTROL ROOM VENTILATION SYSTEM WAS NOT DESIGNED TO | | HAVE A SIMULTANEOUS ACTUATION SIGNAL FROM BOTH UNIT 1 AND UNIT 2 AT THE | | SAME TIME. THE LICENSEE ENTERED TECH SPEC LCO A/S 3.0.3 ON UNIT 2 TO | | TAKE ACTION WITHIN 1 HOUR TO PLACE UNIT 2 IN MODE 4 (HOT SHUTDOWN) WITHIN | | 6 HOURS AND MODE 5 (COLD SHUTDOWN) WITHIN THE FOLLOWING 12 HOURS. | | | | AT 1814, THE LICENSEE RETURNED CONTROL ROOM VENTILATION SYSTEM TO ITS | | NORMAL OPERATING MODE. | | | | AT 1846, THE LICENSEE BLOCKED POWER TO ALL 4 CONTROL ROOM RADIATION | | MONITORS (2 FOR EACH UNIT) AND ENTERED TECH SPEC LCO A/S 3.3.3.1 FOR | | INOPERABLE CONTROL ROOM RADIATION MONITORS. | | | | AT 1952, THE LICENSEE EXITED TECH SPEC LCO A/S 3.0.3 FOR UNIT 2. | | | | THE LICENSEE IS INVESTIGATING THE CAUSE OF THIS EVENT AND DETERMINING | | CORRECTIVE ACTIONS. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+