U.S. Nuclear Regulatory Commission Operations Center Event Reports For 09/27/96 - 09/30/96 ** EVENT NUMBERS ** 31067 31068 31069 31070 31071 31072 31073 31074 31075 +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 31067 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: NORTH ANNA REGION: 2 |NOTIFICATION DATE: 09/27/96 | |UNIT: [ ] [2] [ ] STATE: VA |NOTIFICATION TIME: 00:08 [ET]| |RX TYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 09/26/96 | +------------------------------------------------+EVENT TIME: 21:35[EDT]| |NRC NOTIFIED BY: BECKER |LAST UPDATE DATE: 09/27/96 | |HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |MILTON SHYMLOCK RDO | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | 2 | N N 0 REFUELING | 0 REFUELING | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE PLANT HAD A CONTAINMENT PURGE SYSTEM ISOLATION SIGNAL DUE TO A | | HIGH-HIGH RADIATION SIGNAL FROM THE MANIPULATOR CRANE RAD MONITOR. | | | | THIS OCCURRED DURING THE REACTOR VESSEL HEAD SET EVOLUTION, WHEN THE VESSEL | | HEAD CAME CLOSE TO THE CRANE AND THE HIGH-HIGH SETPOINT (45MR/HR) WAS | | SENSED FOR APPROX. 20 SECONDS BY THE MANIPULATOR CRANE RAD MONITOR. THIS | | GENERATED THE CONTAINMENT PURGE ISOLATION SIGNAL. THE CONTAINMENT PURGE WAS | | RE-ESTABLISHED AT 21:51 WHEN THE REACTOR HEAD WAS BEING LOWERED ONTO THE | | GUIDE STUDS AND THE MANIPULATOR CRANE RAD MONITOR RETURNED TO 5MR/HR. THE | | RI WILL BE INFORMED. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |GENERAL INFORMATION or OTHER | |EVENT NUMBER: 31068 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |LICENSEE: N. CAROLINA DIV OF RAD PROTECTION |NOTIFICATION DATE: 09/27/96 | | CITY: WINSTON-SALEM REGION: 2 |NOTIFICATION TIME: 16:11 [ET]| | COUNTY: STATE: NC |EVENT DATE: 09/27/96 | |LICENSE#: AGREEMENT: Y |EVENT TIME: 15:30[EDT]| | DOCKET: |LAST UPDATE DATE: 09/27/96 | | +-----------------------------+ | |PERSON ORGANIZATION| | |MILTON SHYMLOCK RDO | | | | +------------------------------------------------+ | |NRC NOTIFIED BY: BRIAN HOFFMAN | | |HQ OPS OFFICER: DICK JOLLIFFE | | +------------------------------------------------+ | |EMERGENCY CLASS: NOT APPLICABLE | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------+-----------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - STAINLESS STEEL PIPE SET OFF RAD MONITOR ALARM AT SCRAP METAL YARD - | | | | ED BRADLEY & MIKE BRENNER, BRENNER IRON & METAL COMPANY, REPORTED TO | | BRIAN HOFFMAN, NORTH CAROLINA DIVISION OF RADIATION PROTECTION, THAT A | | 10 FEET LONG, 6 INCH DIAMETER PIECE OF STAINLESS STEEL PIPE HAD BEEN | | RECEIVED AT THEIR SCRAP METAL YARD IN WINSTON-SALEM, NORTH CAROLINA AS | | PART OF A TRUCKLOAD OF SCRAP METAL FROM A PAPER MILL IN NORTH CAROLINA. THE | | PIPE SET OFF THE SCALE MONITOR ALARM AT LEVEL 2 (69-70 RAD). A HAND HELD | | MONITOR READ 7500-8000 COUNTS PER SECOND ON CONTACT WITH THE PIPE. THE PIPE | | WAS UNLOADED FROM THE TRUCK AND BOTH ENDS WERE TAPED SHUT WITH DUCT TAPE. | | THE PIPE IS BEING STORED IN A SECURE AREA AWAY FROM PEOPLE. | | | | SEE HOO LOG FOR CALL BACK TELEPHONE NUMBERS. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 31069 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: WATERFORD REGION: 4 |NOTIFICATION DATE: 09/27/96 | |UNIT: [3] [ ] [ ] STATE: LA |NOTIFICATION TIME: 21:57 [ET]| |RX TYPE: [3] CE |EVENT DATE: 09/27/96 | +------------------------------------------------+EVENT TIME: 20:25[CDT]| |NRC NOTIFIED BY: TERRY SCHRECKENGAST |LAST UPDATE DATE: 09/27/96 | |HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |PHIL HARRELL RDO | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 3 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE NOTIFIED THE LOCAL COAST GUARD AND THE LOCAL SHERIFF THAT | | 1 OF 2 INTAKE STRUCTURE DOLPHIN (STROBE) LIGHTS IS OUT OF SERVICE. | | | | THE LICENSEE WILL REPLACE THE LIGHT. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 31070 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: FERMI REGION: 3 |NOTIFICATION DATE: 09/28/96 | |UNIT: [2] [ ] [ ] STATE: MI |NOTIFICATION TIME: 06:17 [ET]| |RX TYPE: [2] GE-4 |EVENT DATE: 09/28/96 | +------------------------------------------------+EVENT TIME: 04:45[EDT]| |NRC NOTIFIED BY: SANJEEV ARAB |LAST UPDATE DATE: 09/28/96 | |HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |GEOFFREY WRIGHT RDO | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 2 | N N 0 HOT SHUTDOWN | 0 HOT SHUTDOWN | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNEXPECTED TORUS VACUUM BREAKER OPERATION DURING WARMUP OF RHR SYSTEM. | | | | "AT 0445 ON 9/28/96 THE CONTROL ROOM CREW, DURING A PANEL WALKDOWN, NOTED | | THAT PRESSURE IN THE PRIMARY CONTAINMENT (TORUS) DROPPED FROM 2.5 INCHES | | WATER COLUMN TO 0 INCHES WATER COLUMN (0.09 PSIG TO 0 PSIG). AT THE SAME | | TIME THE CREW NOTED THAT THE SUPPRESSION CHAMBER VACUUM BREAKER T23F400K | | WAS OPEN (NOTE THAT THE SETPOINT SHOULD BE 0.5 PSID)." | | | | "THE GREEN CLOSE LIGHTS WERE OFF AND THE RED OPEN LIGHTS WERE NOT ON. THE | | EVOLUTIONS IN PROGRESS DURING THIS EVENT WERE, RHR DIV 1 SUCTION PIPING | | WARMUP IN PREPARATION OF SHUTDOWN COOLING AND THE PRIMARY CONTAINMENT WAS | | PURGING. TORUS WATER LEVEL WAS +1 INCH." | | | | "AT 0456, THE DISCHARGE PATH FOR THE SUCTION WARMUP WAS CLOSED BY CLOSING | | E1150F026B, AT WHICH TIME THE CREW NOTED THAT VACUUM BREAKER T23F400K WENT | | CLOSED (BOTH CLOSE GREEN LIGHT WERE ON)." | | | | THE LICENSEE ATTRIBUTES OPERATION OF THE VACUUM BREAKER VALVE AS A RESPONSE | | TO ADDING WATER TO THE TORUS IN PREPARATION OF ESTABLISHING SHUTDOWN | | COOLING. THE INDIVIDUAL MAKING THIS REPORT WAS UNAWARE IF THE PROCEDURE | | USED BY OPERATORS RECOGNIZED THIS CONDITION. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 31071 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: WATTS BAR REGION: 2 |NOTIFICATION DATE: 09/28/96 | |UNIT: [1] [ ] [ ] STATE: TN |NOTIFICATION TIME: 12:30 [ET]| |RX TYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 09/28/96 | +------------------------------------------------+EVENT TIME: 11:30[EDT]| |NRC NOTIFIED BY: SHELIAH BAKER |LAST UPDATE DATE: 09/28/96 | |HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |MILTON SHYMLOCK RDO | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N N 0 HOT STANDBY | 0 HOT STANDBY | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - SECURITY REPORT - | | | | AT 1130, THE PLANT SECURITY COMPUTER THAT CONTROLS PLANT SECURITY DOOR | | ALARMS AND PLANT PERIMETER ALARMS FAILED. THE LICENSEE IMMEDIATELY | | ESTABLISHED COMPENSATORY MEASURES. | | | | AT 1145, THE LICENSEE RESTORED THE PLANT SECURITY COMPUTER TO OPERABLE | | STATUS AND IS IN THE PROCESS OF VERIFYING OPERABILITY OF PLANT SECURITY | | ALARMS. | | | | THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR. | | | | SEE THE HOO LOG FOR ADDITIONAL DETAILS. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 31072 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: MILLSTONE REGION: 1 |NOTIFICATION DATE: 09/28/96 | |UNIT: [ ] [2] [ ] STATE: CT |NOTIFICATION TIME: 17:15 [ET]| |RX TYPE: [1] GE-3,[2] CE,[3] W-4-LP |EVENT DATE: 09/28/96 | +------------------------------------------------+EVENT TIME: 13:40[EDT]| |NRC NOTIFIED BY: BOB BORCHERT |LAST UPDATE DATE: 09/28/96 | |HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |CLIFFORD ANDERSON RDO | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | 2 | N N 0 COLD SHUTDOWN | 0 COLD SHUTDOWN | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - WELD SPLATTER DISCOVERED ON HPSI PUMP SUCTION PIPE FROM RWST - | | | | WITH UNIT 2 IN MODE 5 (COLD SHUTDOWN) IN A MAINTENANCE OUTAGE, THE LICENSEE | | DISCOVERED WELD SPLATTER ON THE PIPE FROM THE REFUELING WATER STORAGE TANK | | (RWST) TO THE SUCTION OF THE 'A' HIGH PRESSURE SAFETY INJECTION (HPSI) | | PUMP. THE LICENSEE SUSPECTS THAT THE WELD SPLATTER WAS PRESENT SINCE | | ORIGINAL PLANT CONSTRUCTION. | | | | THE LICENSEE DECLARED THE 'A' HPSI PUMP INOPERATIVE, EVEN THOUGH IT IS | | FUNCTIONAL. THE OTHER TWO HPSI PUMPS ARE ALSO INOPERATIVE. TECH SPEC LCO | | A/S 3.1.2.3 PROHIBITS FUEL MOVEMENT WITH ALL THREE HPSI PUMPS INOPERATIVE. | | THE LICENSEE PLANS TO GRIND OUT THE WELD SPLATTER AND REEXAMINE THE PIPE | | BY LIQUID PENETRANT METHOD TO DETERMINE ACCEPTABILITY. | | | | LICENSEE NOTIFIED STATE AND LOCAL OFFICIALS AND THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 31073 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 09/28/96 | |UNIT: [1] [2] [ ] STATE: IL |NOTIFICATION TIME: 21:35 [ET]| |RX TYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 09/28/96 | +------------------------------------------------+EVENT TIME: 16:51[CDT]| |NRC NOTIFIED BY: MIKE FITZPATRICK |LAST UPDATE DATE: 09/29/96 | |HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |GEOFFREY WRIGHT RDO | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N N 0 COLD SHUTDOWN | 0 COLD SHUTDOWN | | 2 | N N 0 REFUELING | 0 REFUELING | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - DIAPHRAGM AREAS OF 38 AIR OPERATED PCIS VALVES < ORIGINAL DESIGN VALUES - | | | | UNIT 1 IS IN CONDITION 4 (COLD SHUTDOWN) IN A MAINTENANCE OUTAGE AND | | UNIT 2 IS IN CONDITION 5 (REFUELING) IN A REFUELING OUTAGE. | | | | THE LICENSEE IDENTIFIED 38 PNEUMATICALLY OPERATED PRIMARY CONTAINMENT | | ISOLATION SYSTEM (PCIS) VALVES ON BOTH UNITS THAT HAVE AN EFFECTIVE | | DIAPHRAGM AREA LESS THAN THE ORIGINAL DESIGN VALUES. THIS CONDITION | | REDUCES THE AVAILABLE CLOSING FORCES WITHIN THE ACTUATOR. POTENTIALLY, | | THE AFFECTED PCIS VALVES WOULD NOT PROVIDE ADEQUATE SYSTEM ISOLATION | | UNDER ACCIDENT CONDITIONS. | | | | IN 05/96, THE LICENSEE IDENTIFIED THIS ISSUE AS A POTENTIAL CONCERN | | DURING THE SEVENTH UNIT 1 REFUELING OUTAGE. | | | | IN 06/96, THE LICENSEE SUBMITTED A 10CFR21 NOTIFICATION TO THE | | ANCHOR-DARLING VALVE COMPANY REGARDING THESE VALVES. | | | | ON 09/20/96, THE LICENSEE RECEIVED CONFIRMATION FROM ANCHOR-DARLING | | OF THE NEED FOR NEW BENCH SET VALUES FOR THESE VALVES. THE LICENSEE, | | WITH ASSISTANCE FROM ANCHOR-DARLING PERSONNEL, WILL CALCULATE NEW SUPPLY | | AIR PRESSURE, VALVE SPRING PRESSURE, ETC, FOR THESE VALVES PRIOR TO | | RESTARTING EITHER UNIT. UNIT 1 IS PRESENTLY SCHEDULED TO RESTART ON | | 10/07/96 AND UNIT 2 IS PRESENTLY SCHEDULED TO RESTART ON 11/19/96. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | | | | * * * UPDATE AT 1436 EDT ON 9/29/96 FROM HENRY TAKEN BY KARSCH * * * | | THE LICENSEE INCORRECTLY REPORTED THE SUBMISSION OF A PART 21 NOTIFICATION | | TO ANCHOR-DARLING. FOLLOWING DISCUSSIONS BETWEEN THE LICENSEE AND | | ANCHOR-DARLING IN JUNE, 1996, ANCHOR-DARLING WAS SUPPOSED TO SUBMIT A PART | | 21 NOTIFICATION, HOWEVER, NO NOTIFICATION HAS BEEN MADE. THE LICENSEE WILL | | FOLLOW UP WITH ANCHOR-DARLING. THE LICENSEE INFORMED THE NRC RESIDENT | | INSPECTOR. R3DO (WRIGHT) NOTIFIED. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 31074 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: FERMI REGION: 3 |NOTIFICATION DATE: 09/29/96 | |UNIT: [2] [ ] [ ] STATE: MI |NOTIFICATION TIME: 12:59 [ET]| |RX TYPE: [2] GE-4 |EVENT DATE: 09/29/96 | +------------------------------------------------+EVENT TIME: 11:30[EDT]| |NRC NOTIFIED BY: BOB GAILLIEZ |LAST UPDATE DATE: 09/29/96 | |HQ OPS OFFICER: RUDY KARSCH +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |GEOFFREY WRIGHT RDO | |AINC 50.72(b)(2)(iii)(C) POT UNCNTRL RAD REL | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 2 | N N 0 COLD SHUTDOWN | 0 COLD SHUTDOWN | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE AS FOUND MAIN STEAM ISOLATION VALVE (MSIV) LEAKAGE FOR THE "A" MAIN | | STEAM LINE EXCEEDED THE TECH SPEC ALLOWABLE LEAK RATE. | | | | THE "A" MSIVs HAD AN AS FOUND LEAK RATE OF 196.2 STANDARD CUBIC FEET PER | | HOUR (SCFH). THE MAXIMUM LEAK RATE ALLOWED BY TECH SPECS IS 100 SCFH FOR | | ALL FOUR MSIVs. THE LICENSEE IS CONTINUING TO TROUBLESHOOT TO IDENTIFY THE | | SOURCE OF THE LEAKAGE. THE TECH SPEC LCO REQUIRES REMAINING IN MODE 4 | | UNTIL THE LEAKAGE IS BELOW 100 SCFH. THE LICENSEE INFORMED THE NRC | | RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 31075 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: MILLSTONE REGION: 1 |NOTIFICATION DATE: 09/29/96 | |UNIT: [1] [ ] [ ] STATE: CT |NOTIFICATION TIME: 23:13 [ET]| |RX TYPE: [1] GE-3,[2] CE,[3] W-4-LP |EVENT DATE: 09/29/96 | +------------------------------------------------+EVENT TIME: 23:10[EDT]| |NRC NOTIFIED BY: PAUL BENYEDA |LAST UPDATE DATE: 09/29/96 | |HQ OPS OFFICER: RUDY KARSCH +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |CLIFFORD ANDERSON RDO | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N N 0 REFUELING | 0 REFUELING | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | A LICENSED INDIVIDUAL EMPLOYED BY THE LICENSEE HAD HIS ACCESS REVOKED WHEN | | HE REPORTED FOR WORK UNDER THE INFLUENCE OF ALCOHOL. FURTHER ACTIONS WILL | | BE DETERMINED. THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. SEE HOO | | LOG FOR FURTHER DETAILS. | +------------------------------------------------------------------------------+