U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/22/96 - 04/23/96 ** EVENT NUMBERS ** 30332 30335 30336 30337 30338 30339 30340 30341 +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30332 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: BROWNS FERRY REGION: 2 |NOTIFICATION DATE: 04/21/96 | |UNIT: [ ] [ ] [3] STATE: AL |NOTIFICATION TIME: 05:50 [ET]| |RX TYPE: [1] GE-4,[2] GE-4,[3] GE-4 |EVENT DATE: 04/21/96 | +------------------------------------------------+EVENT TIME: 03:51[CDT]| |NRC NOTIFIED BY: DONALD C. SMITH |LAST UPDATE DATE: 04/22/96 | |HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |CHARLES CASTO RDO | |ACCS 50.72(b)(1)(iv) ECCS INJECTION | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | | | | 3 | A/R Y 100 POWER OPERATION | 0 HOT STANDBY | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR SCRAM AND AUTOMATIC INITIATION OF HIGH PRESSURE COOLANT | | INJECTION (HPCI) AND REACTOR CORE ISOLATION COOLING (RCIC) AS A RESULT OF | | LOW WATER LEVEL DUE TO THE LOSS OF ONE OF THREE REACTOR FEEDWATER PUMPS | | | | THE 'C' FEEDWATER PUMP TRIPPED FOR UNKNOWN REASONS CAUSING REACTOR WATER | | LEVEL TO DECREASE, AND A LOW LEVEL REACTOR SCRAM FROM 100% POWER OCCURRED | | WHEN WATER LEVEL REACHED THE SCRAM SETPOINT OF -11 INCHES. IN ADDITION, | | BOTH HPCI AND RCIC AUTOMATICALLY INJECTED INTO THE VESSEL WHEN WATER LEVEL | | REACHED -45 INCHES. THE LOWEST WATER LEVEL REACHED BEFORE RECOVERY WAS -47 | | INCHES. THE REACTOR SCRAM CAUSED A TURBINE TRIP, AND THE TURBINE TRIP IN | | TURN CAUSED THE RECIRCULATION PUMPS TO TRIP. ALL RODS FULLY INSERTED DUE | | TO THE REACTOR SCRAM, AND ALL SYSTEMS FUNCTIONED AS REQUIRED. EXPECTED | | GROUP ISOLATIONS 2 (DRYWELL FLOOR AND EQUIPMENT DRAIN ISOLATION VALVES), 3 | | (REACTOR WATER CLEANUP), 6 (PRIMARY AND SECONDARY CONTAINMENT VENTILATION | | ISOLATIONS), AND 8 (TRANSVERSING INCORE PROBES) WERE RECEIVED; AND BOTH THE | | STANDBY GAS TREATMENT AND CONTROL ROOM EMERGENCY VENTILATION SYSTEMS | | AUTOMATICALLY INITIATED AS EXPECTED. NONE OF THE SAFETY RELIEF VALVES | | LIFTED DURING THIS TRANSIENT. | | | | THE UNIT IS CURRENTLY STABLE IN HOT STANDBY. BOTH HPCI AND RCIC HAVE BEEN | | SECURED, AND AT THE TIME OF THIS NOTIFICATION, THE LICENSEE WAS UNSURE OF | | THE AMOUNT OF WATER THAT WAS INJECTED BY THESE SYSTEMS. NORMAL FEEDWATER | | IS CURRENTLY BEING SUPPLIED TO THE VESSEL, THE MAIN STEAM ISOLATIONS VALVES | | ARE OPEN, AND THE CONDENSER IS AVAILABLE AS A HEAT SINK. | | | | THE LICENSEE IS INVESTIGATING THE CAUSE OF THE FEEDWATER PUMP TRIP AND THE | | REASON FOR WATER LEVEL DECREASING TO -47 INCHES. TYPICALLY, WITH A SINGLE | | FEEDWATER PUMP TRIP, WATER LEVEL WOULD BE RECOVERED WITH THE REMAINING TWO | | OPERATING FEEDWATER PUMPS. A RESTART DATE HAS NOT YET BEEN DETERMINED. | | | | THE LICENSEE NOTIFIED THE NRC RESIDENT INSPECTOR AND PLANS TO SUBMIT A | | LICENSEE EVENT REPORT. | | | | * * * 0417 APRIL 22 , 1996, UPDATE FROM SMITH RECEIVED BY TROCINE * * * | | | | DURING THE MORNING STATUS CALL ON APRIL 22, 1996, THE LICENSEE PROVIDED THE | | FOLLOWING ADDITIONAL INFORMATION: | | | | PER THE ABNORMAL OPERATING INSTRUCTIONS, OPERATORS REDUCED REACTOR POWER TO | | APPROXIMATELY 82% TO 85% AFTER THE 'C' REACTOR FEEDWATER PUMP TRIPPED AND | | PRIOR TO THE REACTOR SCRAM. THIS WOULD NORMALLY BE THE APPROPRIATE ACTION | | FOR TWO PUMP OPERATION. HOWEVER, THE REMAINING TWO OPERATING REACTOR | | FEEDWATER PUMPS DID NOT MAINTAIN REACTOR VESSEL WATER LEVEL DUE TO LEAKBY | | ON THE DISCHARGE CHECK VALVE FOR THE 'C' FEEDWATER PUMP FOLLOWING THE PUMP | | TRIP. THE ACTUAL LEVEL DROP WAS RAPID AND QUITE SEVERE. IN ADDITION, BOTH | | HPCI AND RCIC RAN FOR APPROXIMATELY 1-1/2 MINUTES. THE LICENSEE CURRENTLY | | PLANS TO PLACE THE UNIT BACK ON LINE TODAY. | | | | THE NRC OPERATIONS CENTER NOTIFIED THE R2DO (CASTO). | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |HOSPITAL | |EVENT NUMBER: 30335 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |LICENSEE: ADVENTIST HEALTH SYSTEM |NOTIFICATION DATE: 04/22/96 | | CITY: ALTMONTE SPRING REGION: 2 |NOTIFICATION TIME: 16:30 [ET]| | COUNTY: STATE: FL |EVENT DATE: 04/22/96 | |LICENSE#: FL 69-1 AGREEMENT: Y |EVENT TIME: 00:00[EDT]| | DOCKET: |LAST UPDATE DATE: 04/22/96 | | +-----------------------------+ | |PERSON ORGANIZATION| | |CASTO RDO | | | | +------------------------------------------------+ | |NRC NOTIFIED BY: PHILLIP TOMA | | |HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: NOT APPLICABLE | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | +------------------------------------------------+-----------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | STATE OF FLORIDA REPORTED MEDICAL MISADMINISTRATION AT THE ADVENTIST HEALTH | | SYSTEM/SUNBELT INC. FLORIDA HOSPITAL MEDICAL CENTER. | | | | APPROXIMATELY 5-mCi OF I-131 WAS ADMINISTERED TO THE WRONG PATIENT. THE | | STATE OF FLORIDA IS CURRENTLY ATTEMPTING TO CONTACT THE LICENSEE TO | | DETERMINE THE DOSE TO THE PATIENT. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30336 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: SAN ONOFRE REGION: 4 |NOTIFICATION DATE: 04/22/96 | |UNIT: [ ] [2] [3] STATE: CA |NOTIFICATION TIME: 19:11 [ET]| |RX TYPE: [1] W-3-LP,[2] CE,[3] CE |EVENT DATE: 04/22/96 | +------------------------------------------------+EVENT TIME: 14:55[PDT]| |NRC NOTIFIED BY: GREG GIBBS |LAST UPDATE DATE: 04/22/96 | |HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |PELLET RDO | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | 2 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | 3 | N Y 100 POWER OPERATION | 100 POWER OPERATION | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION OF A RELEASE OF APPROXIMATELY 22,440 GALLONS OF | | HIGH-pH WATER INTO THE PLANT DISCHARGE | | | | THE LICENSEE NOTIFIED THE REGIONAL WATER QUALITY CONTROL BOARD REGARDING | | DISCHARGE OF APPROXIMATELY 22,440 GALLONS OF HIGH-pH WATER INTO THE PLANT | | DISCHARGE, WHICH EMPTIES INTO THE PACIFIC OCEAN. THE WATER HAD A pH OF | | 12.6 WITH A LIMIT OF 12.5, AND IT WAS RELEASED BETWEEN 1810 AND 1820 PDT ON | | 04/19/96. THE LICENSEE ALSO NOTIFIED THE CALIFORNIA OFFICE OF EMERGENCY | | SERVICES, DEPARTMENT OF HEALTH SERVICES, AND SAN DIEGO COUNTY. THE NRC | | RESIDENT INSPECTOR WILL BE INFORMED OF THIS EVENT BY THE LICENSEE. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30337 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: FARLEY REGION: 2 |NOTIFICATION DATE: 04/22/96 | |UNIT: [ ] [2] [ ] STATE: AL |NOTIFICATION TIME: 20:01 [ET]| |RX TYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 04/22/96 | +------------------------------------------------+EVENT TIME: 18:22[CDT]| |NRC NOTIFIED BY: GALLE |LAST UPDATE DATE: 04/23/96 | |HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |CASTO RDO | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | 2 | N Y 100 POWER OPERATION | 95 POWER OPERATION | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TECHNICAL SPECIFICATION 3.0.3 SHUTDOWN DUE TO INOPERABILITY OF SIX STEAM | | GENERATOR TUBES (REFER TO EVENT #30328 FOR ADDITIONAL INFORMATION.) | | | | DURING A REANALYSIS OF STEAM GENERATOR TUBE EDDY CURRENT TEST RESULTS, THE | | LICENSEE DISCOVERED SIX TUBES WHICH DO NOT MEET THE F* CRITERIA FOR MINIMUM | | DISTANCE BETWEEN THE ROLL TRANSITION AREA AND THE CLOSEST INDICATION. THE | | LICENSEE DECLARED THE TUBES INOPERABLE IN ACCORDANCE WITH TECHNICAL | | SPECIFICATION 3.4.6, AND ENTERED THE ACTION STATEMENT FOR TECHNICAL | | SPECIFICATION 3.0.3 AS REQUIRED AT 1822 CDT. THE LICENSEE ALSO COMMENCED A | | UNIT SHUTDOWN AT 1834 CDT. | | | | IN ADDITION, THE LICENSEE STATED THAT AN INPO ONSITE VISIT WAS IN PROGRESS | | WHEN INPO REPRESENTATIVES IDENTIFIED CONCERNS WITH THE LICENSEE'S | | INTERPRETATION OF THE F* CRITERIA. THE LICENSEE FURTHER STATED THAT THE | | USE OF ROTATING PANCAKE COIL (RPC) EDDY CURRENT RESULTS WERE PERMITTED BY | | THE NRC IN THE REANALYSIS OF A STEAM GENERATOR TUBE INDICATION ON APRIL 19, | | 1996. HOWEVER, APPLICATION OF RPC RESULTS TO OTHER TUBES HAS RESULTED IN | | THE DETERMINATION THAT THESE SIX TUBES ARE INOPERABLE. | | | | THE NRC RESIDENT INSPECTOR WILL BE INFORMED BY THE LICENSEE. | | | | *** 0035 EDT APRIL 23, 1996, UPDATE FROM OLDFIELD RECEIVED BY TROCINE *** | | | | AT 2308 CDT, THE NRC GRANTED A NOTICE OF ENFORCEMENT DISCRETION TO ALLOW | | UNIT 2 TO CONTINUE POWER OPERATION WITH THE SIX TUBES THAT WERE PREVIOUSLY | | IDENTIFIED TO BE INOPERABLE FOR NOT MEETING THE F* CRITERIA. TECHNICAL | | SPECIFICATION 3.0.3 WAS EXITED AT THAT TIME, AND LOAD REDUCTION HALTED AT | | 35% REACTOR POWER. THE LICENSEE IS CURRENTLY MAKING PREPARATIONS TO RETURN | | TO 100% REACTOR POWER AND PLANS TO CONTINUE STEAM GENERATOR TUBE | | EVALUATIONS TO VERIFY THAT THERE ARE NO FURTHER TUBE PROBLEMS DUE TO | | FAILURE TO MEET THE F* CRITERIA. | | | | THE LICENSEE NOTIFIED THE NRC RESIDENT INSPECTOR. THE NRC OPERATIONS | | CENTER NOTIFIED THE R2DO (CASTO). | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30338 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 04/22/96 | |UNIT: [1] [ ] [ ] STATE: FL |NOTIFICATION TIME: 21:47 [ET]| |RX TYPE: [1] CE,[2] CE |EVENT DATE: 04/22/96 | +------------------------------------------------+EVENT TIME: 21:25[EDT]| |NRC NOTIFIED BY: FIELDS |LAST UPDATE DATE: 04/22/96 | |HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |CASTO RDO | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LICENSEE BORED HOLES THROUGH FIRE BARRIER WITHOUT POSTING CONTINUOUS FIRE | | WATCH. | | | | DURING PERFORMANCE OF A PLANT MODIFICATION, THE LICENSEE DETERMINED THAT | | TWO HOLES HAD BEEN BORED THROUGH THE REACTOR AUXILIARY BUILDING WALL (A | | FIRE BARRIER ASSUMED IN THE FSAR) IN AN AREA WITHOUT CONTINUOUS FIRE | | DETECTION. ALTHOUGH THE LICENSEE HAS A ROVING FIRE WATCH THROUGH THE AREA, | | THE LICENSEE HAS DETERMINED THAT THIS IS INSUFFICIENT AND THAT THIS | | CONDITION PLACES THE UNIT OUTSIDE OF ITS DESIGN BASIS. THE LICENSEE HAS | | POSTED A CONTINUOUS FIRE WATCH IN THE AREA. | | | | THE NRC RESIDENT INSPECTOR WILL BE INFORMED BY THE LICENSEE. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30339 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: SEQUOYAH REGION: 2 |NOTIFICATION DATE: 04/22/96 | |UNIT: [1] [ ] [ ] STATE: TN |NOTIFICATION TIME: 22:59 [ET]| |RX TYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/22/96 | +------------------------------------------------+EVENT TIME: 19:14[EDT]| |NRC NOTIFIED BY: RAY LEIB |LAST UPDATE DATE: 04/22/96 | |HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |CASTO RDO | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POTENTIAL UNANALYZED CONDITION WHILE PERFORMING BLACKOUT TESTING | | | | AS PART OF BLACKOUT TESTING (PROCEDURE SI-126), THE LICENSEE PLACED THE | | '2AA' 6.9-kV SHUTDOWN BOARD ONTO ITS ALTERNATE FEEDER BREAKER, WHICH IS FED | | BY THE 'A' COMMON STATION TRANSFORMER AND WHICH WAS ALSO FEEDING THE '1BB' | | AND '2BB' 6.9-kV SHUTDOWN BOARDS. THE 'A' STATION TRANSFORMER IS DESIGNED | | TO BE LOADED WITH A MAXIMUM OF TWO SHUTDOWN BOARDS. IN ADDITION, THE '2AA' | | EMERGENCY DIESEL GENERATOR WAS PLACED IN TEST MODE AS PART OF THE TEST | | PROCEDURE AND WAS, THEREFORE, UNAVAILABLE. THE LICENSEE STATED THAT THE | | '2AA' SHUTDOWN BOARD WAS LOADED ONTO THE ALTERNATE POWER SUPPLY FOR | | APPROXIMATELY TWO MINUTES DURING THE PERFORMANCE OF THE BLACKOUT TESTING. | | | | AT 2222, THE LICENSEE DETERMINED THAT THE ELECTRICAL CONFIGURATION DURING | | THE TEST MAY HAVE RESULTED IN THE INOPERABILITY OF TWO OFFSITE POWER | | SUPPLIES TO CLASS-1E ELECTRICAL DISTRIBUTION SYSTEMS. THIS CONDITION, WHEN | | COMBINED WITH AN INOPERABLE EMERGENCY DIESEL GENERATOR, WOULD HAVE REQUIRED | | THAT THE UNIT ENTER TECHNICAL SPECIFICATION ACTION STATEMENT 3.0.3. THE | | LICENSEE STATED THAT THIS TEST HAS BEEN PERFORMED IN THE PAST AND THAT THIS | | ISSUE HAS ONLY BEEN RECENTLY DISCOVERED. THE LICENSEE CONTINUES TO | | EVALUATE THE ISSUE. | | | | THE NRC RESIDENT INSPECTOR HAS BEEN INFORMED BY THE LICENSEE. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30340 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: CALVERT CLIFFS REGION: 1 |NOTIFICATION DATE: 04/23/96 | |UNIT: [1] [ ] [ ] STATE: MD |NOTIFICATION TIME: 04:37 [ET]| |RX TYPE: [1] CE,[2] CE |EVENT DATE: 04/23/96 | +------------------------------------------------+EVENT TIME: 04:15[EDT]| |NRC NOTIFIED BY: MONT SECKENS |LAST UPDATE DATE: 04/23/96 | |HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |GENE KELLY RDO | |AMED 50.72(b)(2)(v) OFFSITE MEDICAL | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N N 0 REFUELING | 0 REFUELING | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INDIVIDUAL WITH POSSIBLE HIP AND LEG INJURY TRANSPORTED OFFSITE WHILE | | WEARING CONTAMINATED PROTECTIVE CLOTHING. | | | | AN INDIVIDUAL FELL OFF OF A LADDER IN THE UNIT 1 CONTAINMENT, HIT A | | LANDING, AND ROLLED INTO A PUMP BAY. THE DISTANCE OF THE FALL WAS | | ESTIMATED TO BE APPROXIMATELY 20 FEET TOTAL. THE INDIVIDUAL'S LEG WAS | | POSSIBLY FRACTURED, AND HIS HIP MAY HAVE BEEN INJURED. AS A RESULT, THE | | LICENSEE TRANSPORTED THE INDIVIDUAL VIA AN AMBULANCE TO THE CALVERT | | MEMORIAL HOSPITAL AT 0415. THE INDIVIDUAL WAS STILL WEARING HIS | | CONTAMINATED PROTECTIVE CLOTHING DUE TO THE NATURE OF THE INJURIES. HEALTH | | PHYSICS PERSONNEL ACCOMPANIED THE INDIVIDUAL TO THE HOSPITAL. THE MAXIMUM | | CONTAMINATION ON THE PROTECTIVE CLOTHING WAS ESTIMATED TO BE ABOUT 10,000 | | DISINTEGRATIONS PER MINUTES PER SQUARE CENTIMETER BECAUSE OF THE AREA THAT | | THE INDIVIDUAL WAS WORKING IN. | | | | THE LICENSEE NOTIFIED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30341 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 04/23/96 | |UNIT: [2] [ ] [ ] STATE: NY |NOTIFICATION TIME: 05:18 [ET]| |RX TYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 04/23/96 | +------------------------------------------------+EVENT TIME: 04:19[EDT]| |NRC NOTIFIED BY: JOHN MANSELL |LAST UPDATE DATE: 04/23/96 | |HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |GENE KELLY RDO | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 2 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | STATE AGENCIES NOTIFIED OF OIL SPILL ON SITE. | | | | VENDOR (R.J. GUARRERA) WAS PUMPING OIL FROM A TANKER TRUCK TO THE NORTH GAS | | TURBINE #1 OIL TANK ON THE 15-FOOT ELEVATION, AND THE DISCHARGE HOSE | | DISCONNECTED FROM THE PUMP. AS A RESULT, APPROXIMATELY 20 GALLONS OF OIL | | SPILLED ONTO THE 15-FOOT ELEVATION. THE LEAK WAS IMMEDIATELY STOPPED, AND | | IT WAS CONTAINED ON THE PAVEMENT UNDER AND AROUND THE TRUCK. IT DID NOT | | REACH ANY STORM DRAINS OR THE RIVER. CLEANUP IS CURRENTLY IN PROGRESS AND | | IS ESTIMATED TO BE COMPLETED WITHIN APPROXIMATELY TWO HOURS. THIS EVENT IS | | REPORTABLE BECAUSE THE QUANTITY WAS GREATER THAN FIVE GALLONS. | | | | THE LICENSEE NOTIFIED THE NEW YORK STATE DEPARTMENT OF ENVIRONMENTAL | | CONTROL, THE WESTCHESTER HEALTH DEPARTMENT, INDIAN POINT UNIT 3, AND THE | | NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+