U.S. Nuclear Regulatory Commission Operations Center Event Reports For 02/13/96 - 02/14/96 ** EVENT NUMBERS ** 29974 +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 29974 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: MAINE YANKEE REGION: 1 |NOTIFICATION DATE: 02/14/96 | |UNIT: [1] [ ] [ ] STATE: ME |NOTIFICATION TIME: 00:09 [ET]| |RX TYPE: [1] CE |EVENT DATE: 02/13/96 | +------------------------------------------------+EVENT TIME: 22:28[EST]| |NRC NOTIFIED BY: PETE EBERT |LAST UPDATE DATE: 02/14/96 | |HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |RONALD BELLAMY RDO | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | A/R Y 90 POWER OPERATION | 0 HOT STANDBY | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP ON HIGH STEAM GENERATOR LEVEL DUE TO FAILURE OF A | | MAIN FEEDWATER REGULATING VALVE | | | | AT 22:28 ON FEBRUARY 13, 1996, THE NUMBER 3 MAIN FEEDWATER REGULATING VALVE | | FAILED OPEN WITH THE CONTROL SYSTEM IN AUTOMATIC. STEAM GENERATOR WATER | | LEVEL INCREASED TO APPROXIMATELY 88% (NARROW RANGE), AND THE UNIT | | AUTOMATICALLY TRIPPED ON HIGH FEEDWATER LEVEL. ALL RODS FULLY INSERTED, | | AND ALL SYSTEMS FUNCTIONED AS REQUIRED. THE MAIN FEEDWATER PUMPS | | AUTOMATICALLY TRIPPED, AND EMERGENCY FEEDWATER AUTOMATICALLY INITIATED AS | | DESIGNED. FOLLOWING THE REACTOR PROTECTION SYSTEM ACTUATION, STEAM | | GENERATOR LEVEL DECREASED TO 20% AND WAS SUBSEQUENTLY RECOVERED TO NORMAL | | LEVEL (APPROXIMATELY 60%). THE MAIN STEAM SUPPLY VALVES REMAINED OPEN | | DURING THIS TRANSIENT. | | | | THE UNIT IS CURRENTLY STABLE IN HOT STANDBY, AND THE LICENSEE PLANS TO | | PLACE THE UNIT IN HOT SHUTDOWN. OPERATORS ARE UTILIZING NORMAL CHARGING | | AND MAKEUP, PRESSURIZER HEATERS AND SPRAYS, AND REACTOR COOLANT PUMPS FOR | | PRIMARY INVENTORY, PRESSURE, AND TRANSPORT CONTROL. EMERGENCY FEEDWATER IS | | BEING SUPPLIED TO THE STEAM GENERATORS, AND SECONDARY STEAM IS BEING DUMPED | | TO THE CONDENSER. THE LICENSEE IS CURRENTLY INVESTIGATING THE CAUSE OF THE | | FEEDWATER REGULATING VALVE FAILURE. | | | | THE LICENSEE NOTIFIED THE NRC RESIDENT INSPECTOR AND THE STATE AND MAY | | ISSUE A PRESS RELEASE. | +------------------------------------------------------------------------------+