U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/08/96 - 04/09/96 ** EVENT NUMBERS ** 30240 30244 30247 30248 30249 30250 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30240 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: MCGUIRE REGION: 2 |NOTIFICATION DATE: 04/06/96 | |UNIT: [ ] [2] [ ] STATE: NC |NOTIFICATION TIME: 03:51 [ET]| |RX TYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/06/96 | +------------------------------------------------+EVENT TIME: 02:02[EST]| |NRC NOTIFIED BY: J DIAL |LAST UPDATE DATE: 04/08/96 | |HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |BRUNO URYC RDO | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | 2 | N N 0 HOT SHUTDOWN | 0 HOT SHUTDOWN | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PROCEDURAL INADEQUACY CAUSED THE NUCLEAR SERVICE WATER TO AUXILIARY | | FEEDWATER ASSURED MAKEUP VALVES TO OPEN FOLLOWING CLOSURE OF THE "2B" | | AUXILIARY FEEDWATER PUMP SUCTION VALVE. | | | | NUCLEAR SERVICE WATER TO AUXILIARY FEEDWATER ASSURED MAKEUP VALVE BREAKER | | SHOULD HAVE BEEN OPENED PRIOR TO CLOSING SUCTION VALVE (2CA9). WHEN THE | | SUCTION VALVE WAS CLOSED THE SUCTION PRESSURE DECREASED TO A LOW ENOUGH | | PRESSURE (2 OR 3 psi) TO CAUSE THE ASSURED MAKEUP VALVES TO OPEN. AUXILIARY | | FEEDWATER PUMP "2B" BREAKERS WERE ALREADY OPEN WHEN THE ASSURED MAKEUP | | VALVES OPENED. THE PROCEDURE USED HAD BEEN APPROVED ON 03/27/96. A OF | | COUPLE STEPS IN THE PROCEDURE WERE MISSING. THESE STEPS WOULD HAVE OPENED | | THE BREAKERS TO THE ASSURED MAKEUP VALVES BEFORE CLOSING THE SUCTION VALVE | | (2CA9). PROCEDURE CHANGES ARE BEING MADE TO CORRECT THIS PROBLEM. | | | | RESIDENT INSPECTOR WILL BE INFORMED BY THE LICENSEE. | | | | * * * UPDATE AT 1625 EDT ON 4/8/96 FROM PHILLIPS TAKEN BY KARSCH * * * | | | | AT THE TIME OF THE REPORTED ESF ACTUATION, PUMP "2B" MOTOR HAD BEEN | | PROPERLY REMOVED FROM SERVICE PER PLANT PROCEDURE; THUS, THE ESF ACTUATION | | IS NOT REPORTABLE. THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. R2DO | | (URYC) NOTIFIED BY THE HOO. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30244 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: GRAND GULF REGION: 4 |NOTIFICATION DATE: 04/07/96 | |UNIT: [1] [ ] [ ] STATE: MS |NOTIFICATION TIME: 01:42 [ET]| |RX TYPE: [1] GE-6 |EVENT DATE: 04/07/96 | +------------------------------------------------+EVENT TIME: 00:00[CST]| |NRC NOTIFIED BY: JACOBSON |LAST UPDATE DATE: 04/08/96 | |HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |TOM STETKA RDO | |DDDD 73.71 UNSPECIFIED PARAGRAPH |ED BUTCHER EO | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION |McPEEK (NRR) IAT | | |DAVIDSON (NMSS) IAT | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 99 POWER OPERATION | 99 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SECURITY EVENT - | | | | UNAVAILABILITY OF SECURITY OFFICERS DUE TO STRIKE. NO IMPACT PERCEIVED DUE | | TO POST AUGMENTATION BY SECURITY SUPERVISORY PERSONNEL. | | | | SEE HOO LOG BOOK FOR DETAILS. | | | | ****UPDATE 04/07/96 @ 2334 BY JACOBSON TAKEN BY MACKINNON**** | | | | LICENSEE ISSUED A NEWS RELEASE TO A LOCAL TELEVISION STATION ABOUT THEIR | | SECURITY GUARDS BEING ON STRIKE. LICENSEE NOTIFIED REGION 4 PUBLIC AFFAIRS | | OFFICERS ABOUT THE NEWS RELEASE. RESIDENT INSPECTOR WAS INFORMED BY THE | | LICENSEE OF THIS EVENT. R4DO (TOM STETKA) WAS NOTIFIED BY THE HOO. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30247 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: FARLEY REGION: 2 |NOTIFICATION DATE: 04/08/96 | |UNIT: [ ] [2] [ ] STATE: AL |NOTIFICATION TIME: 03:45 [ET]| |RX TYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 04/08/96 | +------------------------------------------------+EVENT TIME: 00:36[CST]| |NRC NOTIFIED BY: CUMBEE |LAST UPDATE DATE: 04/08/96 | |HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |BRUNO URYC RDO | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | 2 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | "2B" EMERGENCY DIESEL GENERATOR (EDG) INADVERTENTLY RESTARTED AFTER ITS | | ENGINE WAS SHUTDOWN. | | | | DURING THE AUTOSTART TEST OF THE "2B" EDG, IT INADVERTENTLY RESTARTED AFTER | | THE ENGINE WAS SHUTDOWN. INVESTIGATION FOUND THAT THE LICENSEE HAD RESET | | THE EMERGENCY START RELAY PRIOR TO THE TIMING OUT OF THE NON-ESSENTIAL | | ENGINE PROTECTION RELAY. TEST PROCEDURE WILL BE CHANGED TO ENSURE THAT THE | | NON-ESSENTIAL ENGINE PROTECTION RELAY HAS TIMED OUT BEFORE RESETTING THE | | EMERGENCY START RELAY. | | "2B" EDG WAS RETESTED SATISFACTORILY. | | | | RESIDENT INSPECTOR WILL BE INFORMED BY THE LICENSEE OF THIS EVENT. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30248 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: DRESDEN REGION: 3 |NOTIFICATION DATE: 04/08/96 | |UNIT: [1] [ ] [ ] STATE: IL |NOTIFICATION TIME: 15:37 [ET]| |RX TYPE: [1] GE-1,[2] GE-3,[3] GE-3 |EVENT DATE: 04/08/96 | +------------------------------------------------+EVENT TIME: 14:15[CST]| |NRC NOTIFIED BY: STEVE MATTSON |LAST UPDATE DATE: 04/08/96 | |HQ OPS OFFICER: RUDY KARSCH +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: UNUSUAL EVENT +-----------------------------+ |10 CFR SECTION: |BRUCE BURGESS RDO | |AAEC 50.72(a)(1)(i) EMERGENCY DECLARED |CHAFFEE EO | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION |BELCHER FEMA | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N N 0 DECOMMISSIONED | 0 DECOMMISSIONED | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POTENTIALLY CONTAMINATED INJURED INDIVIDUAL TRANSPORTED TO A LOCAL | | HOSPITAL. | | | | A CONTRACTOR WORKER INJURED IN A FALL IN A CONTAMINATED AREA WAS | | TRANSPORTED TO MORRIS HOSPITAL. THE WORKER'S ANTI-Cs WERE CUT AWAY FROM | | HIS BODY, BUT BECAUSE OF HIS INJURY HE WAS NOT ROLLED OVER TO REMOVE THE | | BACK OF HIS CLOTHING. THE CLOTHING MIGHT BE CONTAMINATED. HEALTH PHYSICS | | TECHNICIANS ACCOMPANIED HIM TO THE HOSPITAL. THE LICENSEE INFORMED THE | | NRC RESIDENT INSPECTOR AND THE ILLINOIS DEPARTMENT OF NUCLEAR SAFETY. | | | | * * * UPDATE AT 1706 EDT FROM MATTSON TAKEN BY KARSCH * * * | | | | THE UNUSUAL EVENT TERMINATED AT 1555 CDT. THE SURVEY DETERMINED THAT THE | | INDIVIDUAL WAS NOT CONTAMINATED AND NO CONTAMINATED MATERIALS WERE PRESENT. | | THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR AND APPROPRIATE STATE | | AGENCIES. NRC R3DO (BURGESS), NRC EO (BUTCHER), AND FEMA (BELCHER) | | NOTIFIED. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30249 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: DUANE ARNOLD REGION: 3 |NOTIFICATION DATE: 04/08/96 | |UNIT: [1] [ ] [ ] STATE: IA |NOTIFICATION TIME: 16:15 [ET]| |RX TYPE: [1] GE-4 |EVENT DATE: 04/08/96 | +------------------------------------------------+EVENT TIME: 13:32[CST]| |NRC NOTIFIED BY: TIM ALLEN |LAST UPDATE DATE: 04/08/96 | |HQ OPS OFFICER: RUDY KARSCH +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |BRUCE BURGESS RDO | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HALF GROUP 3 ISOLATION DUE TO A SHORT IN A RAD MONITOR. | | | | AN INSTRUMENT TECHNICIAN WORKING ON THE OFF-GAS PRETREAT RAD MONITOR | | DROPPED AN ELECTRICAL LEAD INTO THE STACK RAD MONITOR. THIS CAUSED A SHORT | | CIRCUIT WHICH BLEW A FUSE, DEENERGIZING THE STACK GAS RAD MONITOR, AND | | INITIATED A HALF GROUP 3 ISOLATION. CONTAINMENT VENTILATION DAMPERS CLOSED | | AND THE STANDBY GAS TREATMENT SYSTEM STARTED. THE FUSE HAS BEEN REPLACED | | AND THE ISOLATION RESET. THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30250 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 04/08/96 | |UNIT: [2] [3] [ ] STATE: PA |NOTIFICATION TIME: 17:00 [ET]| |RX TYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 04/08/96 | +------------------------------------------------+EVENT TIME: 14:20[EST]| |NRC NOTIFIED BY: DAVE LEWIS |LAST UPDATE DATE: 04/08/96 | |HQ OPS OFFICER: RUDY KARSCH +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |THOMAS MOSLAK RDO | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 2 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | 3 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE NOTIFIED THE PENNSYLVANIA DEPARTMENT OF ENVIRONMENTAL | | RESOURCES AND THE U.S. COAST GUARD THAT APPROXIMATELY ONE GALLON OF OIL | | LEAKED FROM THE UNIT 3 OUTER SCREEN STRUCTURE. MOST OF THE SPILL HAS BEEN | | CONTAINED BY A TEMPORARY BOOM. THE LICENSEE INFORMED THE NRC RESIDENT | | INSPECTOR. | +------------------------------------------------------------------------------+ U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/08/96 - 04/09/96 ** EVENT NUMBERS ** 30240 30244 30247 30248 30249 30250 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30240 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: MCGUIRE REGION: 2 |NOTIFICATION DATE: 04/06/96 | |UNIT: [ ] [2] [ ] STATE: NC |NOTIFICATION TIME: 03:51 [ET]| |RX TYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/06/96 | +------------------------------------------------+EVENT TIME: 02:02[EST]| |NRC NOTIFIED BY: J DIAL |LAST UPDATE DATE: 04/08/96 | |HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |BRUNO URYC RDO | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | 2 | N N 0 HOT SHUTDOWN | 0 HOT SHUTDOWN | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PROCEDURAL INADEQUACY CAUSED THE NUCLEAR SERVICE WATER TO AUXILIARY | | FEEDWATER ASSURED MAKEUP VALVES TO OPEN FOLLOWING CLOSURE OF THE "2B" | | AUXILIARY FEEDWATER PUMP SUCTION VALVE. | | | | NUCLEAR SERVICE WATER TO AUXILIARY FEEDWATER ASSURED MAKEUP VALVE BREAKER | | SHOULD HAVE BEEN OPENED PRIOR TO CLOSING SUCTION VALVE (2CA9). WHEN THE | | SUCTION VALVE WAS CLOSED THE SUCTION PRESSURE DECREASED TO A LOW ENOUGH | | PRESSURE (2 OR 3 psi) TO CAUSE THE ASSURED MAKEUP VALVES TO OPEN. AUXILIARY | | FEEDWATER PUMP "2B" BREAKERS WERE ALREADY OPEN WHEN THE ASSURED MAKEUP | | VALVES OPENED. THE PROCEDURE USED HAD BEEN APPROVED ON 03/27/96. A OF | | COUPLE STEPS IN THE PROCEDURE WERE MISSING. THESE STEPS WOULD HAVE OPENED | | THE BREAKERS TO THE ASSURED MAKEUP VALVES BEFORE CLOSING THE SUCTION VALVE | | (2CA9). PROCEDURE CHANGES ARE BEING MADE TO CORRECT THIS PROBLEM. | | | | RESIDENT INSPECTOR WILL BE INFORMED BY THE LICENSEE. | | | | * * * UPDATE AT 1625 EDT ON 4/8/96 FROM PHILLIPS TAKEN BY KARSCH * * * | | | | AT THE TIME OF THE REPORTED ESF ACTUATION, PUMP "2B" MOTOR HAD BEEN | | PROPERLY REMOVED FROM SERVICE PER PLANT PROCEDURE; THUS, THE ESF ACTUATION | | IS NOT REPORTABLE. THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. R2DO | | (URYC) NOTIFIED BY THE HOO. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30244 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: GRAND GULF REGION: 4 |NOTIFICATION DATE: 04/07/96 | |UNIT: [1] [ ] [ ] STATE: MS |NOTIFICATION TIME: 01:42 [ET]| |RX TYPE: [1] GE-6 |EVENT DATE: 04/07/96 | +------------------------------------------------+EVENT TIME: 00:00[CST]| |NRC NOTIFIED BY: JACOBSON |LAST UPDATE DATE: 04/08/96 | |HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |TOM STETKA RDO | |DDDD 73.71 UNSPECIFIED PARAGRAPH |ED BUTCHER EO | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION |McPEEK (NRR) IAT | | |DAVIDSON (NMSS) IAT | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 99 POWER OPERATION | 99 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SECURITY EVENT - | | | | UNAVAILABILITY OF SECURITY OFFICERS DUE TO STRIKE. NO IMPACT PERCEIVED DUE | | TO POST AUGMENTATION BY SECURITY SUPERVISORY PERSONNEL. | | | | SEE HOO LOG BOOK FOR DETAILS. | | | | ****UPDATE 04/07/96 @ 2334 BY JACOBSON TAKEN BY MACKINNON**** | | | | LICENSEE ISSUED A NEWS RELEASE TO A LOCAL TELEVISION STATION ABOUT THEIR | | SECURITY GUARDS BEING ON STRIKE. LICENSEE NOTIFIED REGION 4 PUBLIC AFFAIRS | | OFFICERS ABOUT THE NEWS RELEASE. RESIDENT INSPECTOR WAS INFORMED BY THE | | LICENSEE OF THIS EVENT. R4DO (TOM STETKA) WAS NOTIFIED BY THE HOO. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30247 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: FARLEY REGION: 2 |NOTIFICATION DATE: 04/08/96 | |UNIT: [ ] [2] [ ] STATE: AL |NOTIFICATION TIME: 03:45 [ET]| |RX TYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 04/08/96 | +------------------------------------------------+EVENT TIME: 00:36[CST]| |NRC NOTIFIED BY: CUMBEE |LAST UPDATE DATE: 04/08/96 | |HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |BRUNO URYC RDO | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | 2 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | "2B" EMERGENCY DIESEL GENERATOR (EDG) INADVERTENTLY RESTARTED AFTER ITS | | ENGINE WAS SHUTDOWN. | | | | DURING THE AUTOSTART TEST OF THE "2B" EDG, IT INADVERTENTLY RESTARTED AFTER | | THE ENGINE WAS SHUTDOWN. INVESTIGATION FOUND THAT THE LICENSEE HAD RESET | | THE EMERGENCY START RELAY PRIOR TO THE TIMING OUT OF THE NON-ESSENTIAL | | ENGINE PROTECTION RELAY. TEST PROCEDURE WILL BE CHANGED TO ENSURE THAT THE | | NON-ESSENTIAL ENGINE PROTECTION RELAY HAS TIMED OUT BEFORE RESETTING THE | | EMERGENCY START RELAY. | | "2B" EDG WAS RETESTED SATISFACTORILY. | | | | RESIDENT INSPECTOR WILL BE INFORMED BY THE LICENSEE OF THIS EVENT. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30248 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: DRESDEN REGION: 3 |NOTIFICATION DATE: 04/08/96 | |UNIT: [1] [ ] [ ] STATE: IL |NOTIFICATION TIME: 15:37 [ET]| |RX TYPE: [1] GE-1,[2] GE-3,[3] GE-3 |EVENT DATE: 04/08/96 | +------------------------------------------------+EVENT TIME: 14:15[CST]| |NRC NOTIFIED BY: STEVE MATTSON |LAST UPDATE DATE: 04/08/96 | |HQ OPS OFFICER: RUDY KARSCH +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: UNUSUAL EVENT +-----------------------------+ |10 CFR SECTION: |BRUCE BURGESS RDO | |AAEC 50.72(a)(1)(i) EMERGENCY DECLARED |CHAFFEE EO | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION |BELCHER FEMA | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N N 0 DECOMMISSIONED | 0 DECOMMISSIONED | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POTENTIALLY CONTAMINATED INJURED INDIVIDUAL TRANSPORTED TO A LOCAL | | HOSPITAL. | | | | A CONTRACTOR WORKER INJURED IN A FALL IN A CONTAMINATED AREA WAS | | TRANSPORTED TO MORRIS HOSPITAL. THE WORKER'S ANTI-Cs WERE CUT AWAY FROM | | HIS BODY, BUT BECAUSE OF HIS INJURY HE WAS NOT ROLLED OVER TO REMOVE THE | | BACK OF HIS CLOTHING. THE CLOTHING MIGHT BE CONTAMINATED. HEALTH PHYSICS | | TECHNICIANS ACCOMPANIED HIM TO THE HOSPITAL. THE LICENSEE INFORMED THE | | NRC RESIDENT INSPECTOR AND THE ILLINOIS DEPARTMENT OF NUCLEAR SAFETY. | | | | * * * UPDATE AT 1706 EDT FROM MATTSON TAKEN BY KARSCH * * * | | | | THE UNUSUAL EVENT TERMINATED AT 1555 CDT. THE SURVEY DETERMINED THAT THE | | INDIVIDUAL WAS NOT CONTAMINATED AND NO CONTAMINATED MATERIALS WERE PRESENT. | | THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR AND APPROPRIATE STATE | | AGENCIES. NRC R3DO (BURGESS), NRC EO (BUTCHER), AND FEMA (BELCHER) | | NOTIFIED. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30249 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: DUANE ARNOLD REGION: 3 |NOTIFICATION DATE: 04/08/96 | |UNIT: [1] [ ] [ ] STATE: IA |NOTIFICATION TIME: 16:15 [ET]| |RX TYPE: [1] GE-4 |EVENT DATE: 04/08/96 | +------------------------------------------------+EVENT TIME: 13:32[CST]| |NRC NOTIFIED BY: TIM ALLEN |LAST UPDATE DATE: 04/08/96 | |HQ OPS OFFICER: RUDY KARSCH +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |BRUCE BURGESS RDO | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HALF GROUP 3 ISOLATION DUE TO A SHORT IN A RAD MONITOR. | | | | AN INSTRUMENT TECHNICIAN WORKING ON THE OFF-GAS PRETREAT RAD MONITOR | | DROPPED AN ELECTRICAL LEAD INTO THE STACK RAD MONITOR. THIS CAUSED A SHORT | | CIRCUIT WHICH BLEW A FUSE, DEENERGIZING THE STACK GAS RAD MONITOR, AND | | INITIATED A HALF GROUP 3 ISOLATION. CONTAINMENT VENTILATION DAMPERS CLOSED | | AND THE STANDBY GAS TREATMENT SYSTEM STARTED. THE FUSE HAS BEEN REPLACED | | AND THE ISOLATION RESET. THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30250 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 04/08/96 | |UNIT: [2] [3] [ ] STATE: PA |NOTIFICATION TIME: 17:00 [ET]| |RX TYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 04/08/96 | +------------------------------------------------+EVENT TIME: 14:20[EST]| |NRC NOTIFIED BY: DAVE LEWIS |LAST UPDATE DATE: 04/08/96 | |HQ OPS OFFICER: RUDY KARSCH +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |THOMAS MOSLAK RDO | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 2 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | 3 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE NOTIFIED THE PENNSYLVANIA DEPARTMENT OF ENVIRONMENTAL | | RESOURCES AND THE U.S. COAST GUARD THAT APPROXIMATELY ONE GALLON OF OIL | | LEAKED FROM THE UNIT 3 OUTER SCREEN STRUCTURE. MOST OF THE SPILL HAS BEEN | | CONTAINED BY A TEMPORARY BOOM. THE LICENSEE INFORMED THE NRC RESIDENT | | INSPECTOR. | +------------------------------------------------------------------------------+