U.S. Nuclear Regulatory Commission Operations Center Event Reports For 08/07/96 - 08/08/96 ** EVENT NUMBERS ** 30838 30839 30840 30841 30842 30843 30844 30845 30846 30847 +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30838 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: BROWNS FERRY REGION: 2 |NOTIFICATION DATE: 08/07/96 | |UNIT: [ ] [ ] [3] STATE: AL |NOTIFICATION TIME: 01:37 [ET]| |RX TYPE: [1] GE-4,[2] GE-4,[3] GE-4 |EVENT DATE: 08/06/96 | +------------------------------------------------+EVENT TIME: 20:41[CDT]| |NRC NOTIFIED BY: TIM GOLDEN |LAST UPDATE DATE: 08/07/96 | |HQ OPS OFFICER: RUDY KARSCH +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |MILTON SHYMLOCK RDO | |AINB 50.72(b)(2)(iii)(B) POT RHR INOP | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | | | | | 3 | N Y 100 POWER OPERATION | 100 POWER OPERATION | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF POWER TO THE SENSORS FOR DIVISION 1 ECCS RENDER SEVERAL SAFETY | | FUNCTIONS INOPERABLE. THE MOST RESTRICTIVE TECH SPEC LCO IS 6 HOURS DUE TO | | HPCI INOPERABILITY. | | | | THE DIVISION 1 ECCS ANALOG TRIP UNIT INVERTER LOST POWER DUE TO A BLOWN | | FUSE. THE ECCS DIVISION 1 INVERTER SUPPLIES POWER TO 2 OF 4 CHANNELS OF | | DRYWELL PRESSURE AND REACTOR WATER LEVEL SENSORS. THESE SENSORS FEED BOTH | | DIVISIONS OF INITIATION LOGIC FOR ALL ECCS SYSTEMS (RHR, CORE SPRAY, HPCI, | | ADS, AND DIESEL GENERATORS). OTHER SENSORS FOR REACTOR PRESSURE AND | | CONTAINMENT PARAMETERS ARE ALSO SUPPLIED BY THIS INVERTER AS IS THE RCIC | | FLOW CONTROLLER. THE REMAINING INVERTER IS SUFFICIENT TO INITIATE THE | | LOGIC OF ALL ECCS DIVISIONS. ALL OF THE ABOVE SYSTEMS WOULD HAVE FULFILLED | | THEIR DESIGN FUNCTIONS WITH THE EXCEPTION OF RCIC AND LOOP 1 CORE SPRAY DUE | | TO LOSS OF THE LOW PRESSURE PERMISSIVE FOR THE INJECTION VALVE. THE | | ATWS/RPT LOGIC WAS ALSO MADE INOPERABLE RESULTING IN A 72-HOUR LCO PER TECH | | SPEC TABLE 3.2.L. PER TECH SPEC 3.5.G ADS WAS DECLARED INOPERABLE | | RESULTING IN A 12-HOUR LCO. ALL AFFECTED ECCS SYSTEMS AND RCIC WERE | | DECLARED INOPERABLE DUE TO THE LOSS OF LOGIC IN ACCORDANCE WITH TECH SPEC | | TABLE 3.2.B. THE LOSS OF HPCI TRIGGERS A 6-HOUR LCO AND IS REPORTABLE DUE | | TO THE LOSS OF A SINGLE TRAIN SAFETY SYSTEM. THE LOSS OF POWER TO THE | | INVERTER DOES NOT CAUSE THE PARTIAL ACTIVATION OF THE TRIP LOGIC. THE | | LICENSEE IS TROUBLESHOOTING THE ROOT CAUSE OF THE BLOWN FUSE AND IS WORKING | | TO RESTORE POWER TO THE INVERTER. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |OTHER NUCLEAR MATERIAL | |EVENT NUMBER: 30839 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |LICENSEE: H. C. NUTTING COMPANY |NOTIFICATION DATE: 08/07/96 | | CITY: CINCINATTI REGION: 3 |NOTIFICATION TIME: 10:20 [ET]| | COUNTY: HAMILTON STATE: OH |EVENT DATE: 08/07/96 | |LICENSE#: 34-18882-01 AGREEMENT: N |EVENT TIME: 07:00[EDT]| | DOCKET: |LAST UPDATE DATE: 08/07/96 | | +-----------------------------+ | |PERSON ORGANIZATION| | |BRUCE BURGESS RDO | | | | +------------------------------------------------+ | |NRC NOTIFIED BY: BECKER | | |HQ OPS OFFICER: LEIGH TROCINE | | +------------------------------------------------+ | |EMERGENCY CLASS: NOT APPLICABLE | | |10 CFR SECTION: | | |BAB2 20.2201(a)(1)(ii) LOST/STOLEN LNM>10X | | | | | | | | | | | | | | +------------------------------------------------+-----------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | H. C. NUTTING COMPANY OF CINCINNATI, OHIO, REPORTED A STOLEN TROXLER | | NUCLEAR DENSITY GAUGE. | | | | BETWEEN 2300 ON AUGUST 6, 1996, AND 0700 ON AUGUST 7, 1996, A VEHICLE | | CONTAINING A TROXLER NUCLEAR DENSITY GAUGE WAS STOLEN FROM THE FRONT OF A | | LICENSEE TECHNICIAN'S RESIDENCE. THE TROXLER GAUGE AND THE CASE CONTAINING | | THE GAUGE WERE BOTH LOCKED AND PLACARDED WITH RADIOACTIVE SYMBOLS, AND THE | | CASE WAS LOCATED IN THE REAR COMPARTMENT OF A JEEP LAREDO. THE CASE WAS | | ALSO CAMOUFLAGED WITH A CURTAIN OVER IT. THE INVESTIGATING POLICE OFFICER | | BELIEVED THAT THE THIEF WAS INTERESTED IN THE VEHICLE RATHER THAN THE | | TROXLER GAUGE. | | | | THE LICENSEE NOTIFIED THE LOCAL POLICE DEPARTMENT AND NRC REGION 3 | | (SIMMONS). THE LICENSEE ALSO PLANS TO NOTIFY BOTH LOCAL NEWS PAPERS, THE | | LOCAL RADIO STATION, THE CITY OF CINCINNATI HEALTH DEPARTMENT, AND THE | | HAMILTON COUNTY HEALTH DEPARTMENT. (REFER TO THE HOO LOG FOR THE | | LICENSEE'S TELEPHONE NUMBER AND ADDRESS.) | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |OTHER NUCLEAR MATERIAL | |EVENT NUMBER: 30840 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |LICENSEE: DR. LUIZ FERNANDEZ |NOTIFICATION DATE: 08/07/96 | | CITY: REGION: 2 |NOTIFICATION TIME: 12:55 [ET]| | COUNTY: STATE: PR |EVENT DATE: 08/07/96 | |LICENSE#: 52-25114-01 AGREEMENT: N |EVENT TIME: 12:00[AT ]| | DOCKET: |LAST UPDATE DATE: 08/07/96 | | +-----------------------------+ | |PERSON ORGANIZATION| | |MILTON SHYMLOCK RDO | | | | +------------------------------------------------+ | |NRC NOTIFIED BY: WANDA MARTINEZ | | |HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: NOT APPLICABLE | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------+-----------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MEDICAL MISADMINISTRATION | | | | SIX PATIENTS RECEIVED A DOSE 26% SMALLER THAN WAS PRESCRIBED. THE CAUSE OF | | THE MISADMINISTRATION WAS THE USE OF AN OLD Sr-90 SOURCE. THE DECAY OF THE | | SOURCE WAS NOT TAKEN INTO ACCOUNT WHEN CALCULATING THE DOSES. THESE DOSES | | WERE DELIVERED IN 1994 AND 1995 WITH A SOURCE ORIGINALLY DELIVERED IN 1982. | | THE MISADMINISTRATIONS WERE DISCOVERED BY AN NRC INSPECTOR WHO IS CURRENTLY | | REVIEWING THE DOCTOR'S RECORDS. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30841 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: MAINE YANKEE REGION: 1 |NOTIFICATION DATE: 08/07/96 | |UNIT: [1] [ ] [ ] STATE: ME |NOTIFICATION TIME: 15:07 [ET]| |RX TYPE: [1] CE |EVENT DATE: 08/07/96 | +------------------------------------------------+EVENT TIME: 14:25[EDT]| |NRC NOTIFIED BY: PETE EBERT |LAST UPDATE DATE: 08/07/96 | |HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |JAMES NOGGLE RDO | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N N 0 HOT STANDBY | 0 HOT STANDBY | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FEEDWATER REGULATING VALVE BYPASS VALVES MIGHT NOT CLOSE WHEN REQUIRED | | | | ON 7/20/96, WHILE SHUTDOWN, LEAKAGE PAST THE #3 MAIN FEED REGULATING VALVE | | BYPASS VALVE WAS OBSERVED WITH THE VALVE POSITIONER SET IN THE SHUT | | POSITION. SUBSEQUENT TESTING OF ALL 3 MAIN FEED REGULATING VALVE BYPASS | | VALVES DETERMINED THAT ALL 3 VALVES LEAKED BY TO VARYING DEGREES. THE | | SAFETY FUNCTION OF THE BYPASS VALVES IS TO SHUT OFF FEED TO THE STEAM | | GENERATOR IN THE EVENT OF A STEAM LINE BREAK IN ORDER TO PREVENT EXCESSIVE | | COOLDOWN. | | | | THE BYPASS VALVES ARE AIR-TO-OPEN AND SPRING-TO-CLOSE VALVES. WHEN THE | | LEAKAGE WAS OBSERVED, THE DESIGN BASIS FOR THE SPRING FORCE WAS | | INVESTIGATED TO DETERMINE IF THE CONDITION WAS THE RESULT OF SET POINT | | DRIFT OR A DISCREPANT SETTING. THE BASIS FOR THE SETTING COULD NOT BE | | RECOVERED AND ENGINEERING DEVELOPED A CALCULATION FOR THE REQUIRED | | SETPOINT. AT 1425 ON 8/7/96, THE CONTROL ROOM WAS NOTIFIED THAT THE | | ORIGINAL SPRING SETTING WAS NOT SUFFICIENT TO SHUT OFF FLOW UNDER WORST | | CASE DESIGN BASIS CONDITIONS WHEN THE FEED TRAIN TRIP SIGNAL IS RECEIVED. | | | | THE BYPASS VALVES ARE BEING RESET WITH A NEW SPRING SETTING WHICH MEETS THE | | WORST CASE DESIGN BASIS CONDITION. | | | | THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |HOSPITAL | |EVENT NUMBER: 30842 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |LICENSEE: UNIVERSITY OF CONN HEALTH CENTER |NOTIFICATION DATE: 08/07/96 | | CITY: FARMINGTON REGION: 1 |NOTIFICATION TIME: 15:55 [ET]| | COUNTY: STATE: CT |EVENT DATE: 08/07/96 | |LICENSE#: AGREEMENT: N |EVENT TIME: 12:00[EDT]| | DOCKET: |LAST UPDATE DATE: 08/07/96 | | +-----------------------------+ | |PERSON ORGANIZATION| | |JAMES NOGGLE RDO | | | | +------------------------------------------------+ | |NRC NOTIFIED BY: KEN PRICE | | |HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: NOT APPLICABLE | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------+-----------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MEDICAL MISADMINISTRATION | | | | A PATIENT RECEIVING TREATMENTS TO THE LUNG WAS GIVEN A DOSE OF 300 RADS | | VICE THE 150 RADS PRESCRIBED IN THE FRACTION. A TOTAL OF 3450 RADS WAS TO | | BE GIVEN IN 22 FRACTIONS. THIS WAS THE 21ST FRACTION. THE DOSE WAS GIVEN | | USING Co-60. THE CAUSE OF THE MISADMINISTRATION WAS INPROPER DATA ENTRY AND | | FAILURE TO VERIFY THE CALCULATIONS USED. | | | | NO CLINICAL SYMPTOMS ARE EXPECTED BECAUSE OF THIS MISADMINISTRATION. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |OTHER NUCLEAR MATERIAL | |EVENT NUMBER: 30843 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |LICENSEE: JOHNSTON ISLAND (US ARMY) |NOTIFICATION DATE: 08/07/96 | | CITY: REGION: 4 |NOTIFICATION TIME: 16:06 [ET]| | COUNTY: STATE: HI |EVENT DATE: 07/16/96 | |LICENSE#: 12-00722-13 AGREEMENT: N |EVENT TIME: 12:00[AH ]| | DOCKET: |LAST UPDATE DATE: 08/07/96 | | +-----------------------------+ | |PERSON ORGANIZATION| | |BRUCE BURGESS RDO | | | | +------------------------------------------------+ | |NRC NOTIFIED BY: BETTY PETERSON | | |HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: NOT APPLICABLE | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------+-----------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | EIGHTEEN CELL MODULES CONTAINING Am-241 WERE LOST | | | | EACH CELL MODULE CONTAINS 250 ęCi OF Am-241. THE CELLS ARE USED IN A | | CHEMICAL AGENT ALARM SYSTEM. EACH SOURCE IS CONTAINED IN A PERFORATED | | METAL BOX WITH A WARNING ON THE OUTSIDE THAT THE CONTENTS ARE RADIOACTIVE. | | REGION III HAD BEEN PREVIOUSLY NOTIFIED OF THIS EVENT IN THE MIDDLE OF | | JULY. | | | | THE CELLS WERE LAST SIGHTED ON JOHNSTON ISLAND (SOUTH OF THE HAWAIIAN | | ISLANDS) IN FEBRUARY OF THIS YEAR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |OTHER NUCLEAR MATERIAL | |EVENT NUMBER: 30844 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |LICENSEE: USAF |NOTIFICATION DATE: 08/07/96 | | CITY: REGION: 0 |NOTIFICATION TIME: 16:15 [ET]| | COUNTY: STATE: |EVENT DATE: 08/05/96 | |LICENSE#: AGREEMENT: |EVENT TIME: 12:00[ ]| | DOCKET: |LAST UPDATE DATE: 08/07/96 | | +-----------------------------+ | |PERSON ORGANIZATION| | |JOHN PELLET RDO | | | | +------------------------------------------------+ | |NRC NOTIFIED BY: CAPT MONTGOMERY | | |HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: NOT APPLICABLE | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------+-----------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AN 8 ęCi Am-241 SOURCE WAS LOST WHEN AN AIR FORCE PLANE CRASHED IN SAUDI | | ARABIA. THE CRASH SITE HAS BEEN SECURED AND NO PERSONNEL EXPOSURES ARE | | EXPECTED TO OCCUR. THE SOURCE WAS CONTAINED IN THE PLANES LANTIRN POD. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |GENERAL INFORMATION or OTHER | |EVENT NUMBER: 30845 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |LICENSEE: TSI |NOTIFICATION DATE: 08/07/96 | | CITY: ST. PAUL REGION: 3 |NOTIFICATION TIME: 17:45 [ET]| | COUNTY: STATE: MN |EVENT DATE: 08/07/96 | |LICENSE#: AGREEMENT: N |EVENT TIME: 12:00[CDT]| | DOCKET: |LAST UPDATE DATE: 08/07/96 | | +-----------------------------+ | |PERSON ORGANIZATION| | | | | | | +------------------------------------------------+VERN HODGE NRR | |NRC NOTIFIED BY: TSI | | |HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: NOT APPLICABLE | | |10 CFR SECTION: | | |CCCC 21.21 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +------------------------------------------------+-----------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PART 21 REPORTED BY TSI, ENVIRONMENTAL MEASUREMENTS AND CONTROLS DIVISION | | | | TSI REPORTED THAT SOME OF THEIR INSTRUMENTS MAY NOT PERFORM CORRECTLY IN | | ELEVATED TEMPERATURE AND HIGH HUMIDITY ENVIRONMENTS. THE FOLLOWING | | INSTRUMENTS MAY HAVE THIS PROBLEM. | | | | VELOCICALC MODELS 8355, 8357, 8360, 8382, 8383, AND 8388 WITH SERIAL | | NUMBERS BEGINNING WITH THE DIGITS 604 THROUGH 606 OR 9604 THROUGH 9606 | | | | VELOCICHECK MODELS 8330, 8340 WITH SERIAL NUMBERS BEGINNING WITH THE DIGITS | | 9601 THROUGH 9606 | | | | ACCUBALANCE MODEL 8370 WITH SERIAL NUMBERS BEGINNING WITH THE DIGITS 601 | | THROUGH 606 | | | | DP-CALC MODELS 8702, 8704 WITH SERIAL NUMBERS BEGINNING WITH THE DIGITS | | 9604 THROUGH 9606 | | | | TSI WILL SEND THIS INFORMATION TO ALL IDENTIFIED OWNERS OF THE INSTRUMENTS | | LISTED ABOVE. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30846 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: GINNA REGION: 1 |NOTIFICATION DATE: 08/07/96 | |UNIT: [1] [ ] [ ] STATE: NY |NOTIFICATION TIME: 22:26 [ET]| |RX TYPE: [1] W-2-LP |EVENT DATE: 08/07/96 | +------------------------------------------------+EVENT TIME: 20:11[EDT]| |NRC NOTIFIED BY: MIKE RUBY |LAST UPDATE DATE: 08/07/96 | |HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |JAMES NOGGLE RDO | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N N 0 HOT STANDBY | 0 HOT STANDBY | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ESF ACTUATION - AUTOSTART OF BOTH AFW PUMPS | | | | A REALIGNMENT OF THE AUXILIARY FEEDWATER SYSTEM WAS IN PROGRESS TO SATISFY | | TECH SPEC REQUIREMENTS. AN AUTOSTART OF BOTH AFW PUMPS OCCURRED DUE TO A | | MECHANICAL ROD IN A MAIN FEED PUMP BREAKER NOT PROPERLY MAKING UP AUXILIARY | | CONTACTS. THE BREAKER WAS IN A TEST POSITION DURING THIS PROCESS AND THE | | AFW PUMPS SHOULD NOT HAVE STARTED. | | | | THE PROBLEM WITH THE MAIN FEEDWATER PUMP BREAKER HAS BEEN CORRECTED AND THE | | AFW PUMPS RETURNED TO THEIR PRE TEST CONDITION. ONE PUMP IS BEING USED TO | | MAINTAIN STEAM GENERATOR LEVEL WITH THE PLANT IN MODE 3. | | | | THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 30847 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 08/08/96 | |UNIT: [1] [2] [ ] STATE: IL |NOTIFICATION TIME: 03:11 [ET]| |RX TYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 08/08/96 | +------------------------------------------------+EVENT TIME: 01:20[CDT]| |NRC NOTIFIED BY: JAY HOUSTON |LAST UPDATE DATE: 08/08/96 | |HQ OPS OFFICER: RUDY KARSCH +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | 2 | N Y 95 POWER OPERATION | 95 POWER OPERATION | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | A CONTRACTOR WAS LEFT UNESCORTED IN THE CONTRACTOR'S LUNCH ROOM FOR | | APPROXIMATELY ONE HOUR. THE INDIVIDUAL WAS ESCORTED OFF SITE. THE | | LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+