U.S. Nuclear Regulatory Commission Operations Center Event Reports For 03/02/95 - 03/03/95 ** EVENT NUMBERS ** 28308 28464 28465 28466 28467 28468 28469 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 28308 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: ROBINSON REGION: 2 |NOTIFICATION DATE: 01/31/95 | |UNIT: [2] [ ] [ ] STATE: SC |NOTIFICATION TIME: 06:55 [ET]| |RX TYPE: [2] W-3-LP |EVENT DATE: 01/31/95 | +------------------------------------------------+EVENT TIME: 03:03[EST]| |NRC NOTIFIED BY: DOUG WINTERS |LAST UPDATE DATE: 03/02/95 | |HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |GEORGE AL BELISLE RDO | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 2 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | EDG "A" STARTED UNEXPECTEDLY WHEN PLACING THE LOCAL/REMOTE SWITCH TO REMOTE | | | | EDG "A" WAS BEING RUN TO TEST ITS FUEL OIL TRANSFER PUMP. AFTER COMPLETION | | OF THE TEST THE EDG WAS STOPPED IAW OP-604. WHEN THE LOCAL/REMOTE SWITCH | | WAS PLACED IN REMOTE, THE DIESEL RESTARTED. THE DIESEL WAS SUBSEQUENTLY | | STOPPED. THE LICENSEE DOES NOT CONSIDER THIS A VALID ESF ACTUATION BUT IS | | REPORTING THE EVENT BECAUSE THE RESPONSE WAS UNEXPECTED. THE LICENSEE HAS | | CONCLUDED THE DIESEL WOULD HAVE BEEN AVAILABLE TO SUPPORT AN ESF ACTUATION | | & SUPPLY POWER TO THE EMERGENCY BUS. THE CAUSE OF THE MALFUNCTION IS BEING | | INVESTIGATED. | | | | EDG "A" HAS BEEN DECLARED OPERABLE. THOUGH THE FAULT HAS NOT BEEN | | SPECIFICALLY IDENTIFIED, THE LICENSEE CONSIDERS THE DIESEL OPERABLE BECAUSE | | NO ALARM EXISTS IN THE CONTROL ROOM WHEN THE LOCAL/REMOTE SWITCH IS PLACED | | IN REMOTE. A BARRING OVER PROCEDURE IS NORMALLY PERFORMED AFTER STOPPING | | THE DIESEL AND THIS PROCEDURE WAS PERFORMED. THIS PROCEDURE EXERCISES THE | | LOCAL/REMOTE SWITCH. WHEN THE SWITCH WAS PLACED IN LOCAL, THE EXPECTED | | ALARM WAS RECEIVED IN THE CONTROL ROOM. WHEN THE SWITCH WAS TAKEN BACK TO | | REMOTE, THE ALARM CLEARED AND THE DIESEL DID NOT RE-START. | | | | THE LICENSEE WILL INFORM THE NRC RESIDENT INSPECTOR. | | | | ****UPDATE 03/02/95 @ 1600EST BY CROOK TAKEN BY MACKINNON*** | | LICENSEE IS RETRACTING THIS EVENT BECAUSE "A" EDG HAD BEEN PROPERLY REMOVED | | FROM SERVICE WHEN IT AUTOMATICALLY STARTED ON A NON VALID ACTUATION SIGNAL. | | R2DO (BILL CLINE) NOTIFIED | | RESIDENT INSPECTOR WAS INFORMED BY THE LICENSEE. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 28464 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 03/02/95 | |UNIT: [1] [ ] [ ] STATE: NY |NOTIFICATION TIME: 16:06 [ET]| |RX TYPE: [1] GE-4 |EVENT DATE: 03/02/95 | +------------------------------------------------+EVENT TIME: 13:14[EST]| |NRC NOTIFIED BY: ZAREMBA |LAST UPDATE DATE: 03/02/95 | |HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |HAROLD GRAY RDO | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N N 0 REFUELING | 0 REFUELING | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NOTIFIED NEW YORK STATE DEPARTMENT OF ENVIRONMENTAL CONSERVATION THAT THEIR | | SEWAGE TREATMENT EFFLUENT WAS GREATER THAN THE ALLOWED DISCHARGE LIMIT. | | | | LICENSEE NOTIFIED NEW YORK STATE DEPARTMENT OF ENVIRONMENTAL CONSERVATION | | THAT THE RESULTS OF THEIR SEWAGE TREATMENT PLANT EFFLUENT SAMPLE TAKEN ON | | 02/21/95 FOR FECAL COLIFORM EXCEEDED THEIR DISCHARGE LIMIT OF 400 COLONIES | | (SAMPLE WAS 600 COLONIES). BACKUP SAMPLE TAKEN ON 02/28/95 WAS WITHIN THE | | DISCHARGE LIMIT. | | | | RESIDENT INSPECTOR WAS INFORMED BY THE LICENSEE. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 28465 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: MAINE YANKEE REGION: 1 |NOTIFICATION DATE: 03/02/95 | |UNIT: [1] [ ] [ ] STATE: ME |NOTIFICATION TIME: 16:43 [ET]| |RX TYPE: [1] CE |EVENT DATE: 03/02/95 | +------------------------------------------------+EVENT TIME: 16:00[EST]| |NRC NOTIFIED BY: GRIMARD |LAST UPDATE DATE: 03/02/95 | |HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |HAROLD GRAY RDO | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N N 0 REFUELING | 0 REFUELING | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LICENSEE DECLARED ALL THREE (THEY HAVE TWO CONTAINMENT SPRAY PUMPS AND A | | SWING PUMP WHICH CAN BE USED FOR CONTAINMENT SPRAY) OF THEIR CONTAINMENT | | SPRAY PUMPS INOPERABLE. | | | | CONTAINMENT SPRAY PUMP FLOW TEST MEASUREMENTS WERE REVIEWED BY ENGINEERING. | | ENGINEERING COULD NOT DETERMINE IF EACH CONTAINMENT SPRAY PUMP COULD | | DISCHARGE 3700gpm AT A DISCHARGE PRESSURE OF 140psig. PAST CONTAINMENT | | SPRAY PUMP FLOW TEST MEASUREMENTS WERE PERFORMED AT A DISCHARGE PRESSURE | | BETWEEN 100psig TO 110psig AND NOT AT A DISCHARGE PRESSURE OF 140psig. ONE | | OF THE TEST ACCEPTANCE CRITERIA IS THAT EACH CONTAINMENT SPRAY PUMP WILL | | DISCHARGE 3700gpm AT A DISCHARGE PRESSURE OF 140psig (LICENSEE DID NOT KNOW | | WHAT THIS TEST ACCEPTANCE CRITERIA WAS BASED UPON AND WHY THEY HAD NEVER | | FOUND THIS PROBLEM BEFORE). ENGINEERING WILL REPERFORM THE CONTAINMENT | | SPRAY PUMP TEST AT A DISCHARGE PRESSURE OF 140psig TO DETERMINE IF EACH | | CONTAINMENT SPRAY PUMP DISCHARGES ò 3700gpm. LICENSEE IS NOT IN ANY TECH | | SPEC ACTION STATEMENT. | | | | RESIDENT INSPECTOR WAS INFORMED BY THE LICENSEE. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 28466 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: BRAIDWOOD REGION: 3 |NOTIFICATION DATE: 03/02/95 | |UNIT: [1] [ ] [ ] STATE: IL |NOTIFICATION TIME: 16:51 [ET]| |RX TYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/02/95 | +------------------------------------------------+EVENT TIME: 12:30[CST]| |NRC NOTIFIED BY: ED STEFAN |LAST UPDATE DATE: 03/02/95 | |HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |MCCORMICKBARGER RDO | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N N 0 COLD SHUTDOWN | 0 COLD SHUTDOWN | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DURING STEAM GENERATOR TUBE INSERVICE INSPECTION, STEAM GENERATOR "1C" WAS | | CLASSIFIED AS CATEGORY C-3. STEAM GENERATORS "1A", "1B", & "1D" TUBE | | INSERVICE INSPECTION DATA IS BEING REVIEWED. | | | | THE FOLLOWING TEXT IS FROM A FACSIMILE. | | | | "ON FEBRUARY 23, 1995 A STEAM GENERATOR (SG) TUBE INSERVICE INSPECTION WAS | | INITIATED ON BRAIDWOOD UNIT 1 IN ACCORDANCE WITH TECHNICAL SPECIFICATION | | SURVEILLANCE REQUIREMENT (TTSR) 4.4.5.0. | | | | THE INITIAL SAMPLE SIZE OF ALL AVAILABLE TUBES WAS SELECTED. | | | | TTSR 4.4.5.2.c. REQUIRES THAT THE RESULTS OF EACH SAMPLE INSPECTION BE | | CLASSIFIED INTO ONE OF THREE CATEGORIES. A SG WILL BE CLASSIFIED IN | | CATEGORY C-3 IF MORE THAN 10% OF THE TOTAL TUBES INSPECTED ARE DEGRADED OR | | MORE THAN 1% OF THE INSPECTED TUBE ARE DEFECTIVE. A SG TUBE IS CONSIDERED | | DEGRADED IF IT HAS AN IMPERFECTION OF GREATER THAN OR EQUAL TO 20% NOMINAL | | TUBE WALL THICKNESS. A SG TUBE IS CONSIDERED DEFECTIVE IF IT HAS AN | | IMPERFECTION OF GREATER THAN OR EQUAL TO 40% NOMINAL TUBE WALL THICKNESS IN | | NON-TUBE SUPPORT PLATE REGIONS. IN THE TUBE SUPPORT PLATE REGIONS, A TUBE | | IS CONSIDERED TO BE DEFECTIVE IF IT CONTAINS AN INDICATION GREATER THAN 2.7 | | VOLTS OR IF CONTAINS AN INDICATION GREATER THAN 1 VOLT BUT LESS THAN OR | | EQUAL TO 2.7 VOLTS AND IT IS CONFIRMED BY ROTATING PANCAKE COIL (RPC) | | INSPECTION. ON MARCH 2, 1995 AT 12:30 HOURS, THE RESULTS OF THE SAMPLE | | INSPECTION RESULTED IN SG 1C BEING CLASSIFIED INTO CATEGORY C-3 BASED ON | | 319 OF THE 4212 INSERVICE TUBES BEING DEFECTIVE. MOST OF THESE TUBES ARE | | DUE TO INDICATIONS AT THE HOT LEG TUBE SUPPORT PLATE REGION. | | TECHNICAL SPECIFICATION TABLE 4.4-2 REQUIRES NRC NOTIFICATION PURSUANT TO | | 10 CFR 50.72 (b) (2) (i) FOR ANY SG CLASSIFICATION IN CATEGORY C-3. | | | | AN ESTIMATED 12 ADDITIONAL TUBES WILL REQUIRE TO BE PLUGGED IN THE 1C SG | | ONCE FURTHER REVIEW IS COMPLETED" END OF TEXT. | | | | RESIDENT INSPECTOR WAS INFORMED BY THE LICENSEE. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 28467 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 03/02/95 | |UNIT: [1] [ ] [ ] STATE: OH |NOTIFICATION TIME: 18:02 [ET]| |RX TYPE: [1] GE-6 |EVENT DATE: 03/02/95 | +------------------------------------------------+EVENT TIME: 15:45[EST]| |NRC NOTIFIED BY: ALAN RABENOLD |LAST UPDATE DATE: 03/02/95 | |HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |MCCORMICKBARGER RDO | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 100 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR WATER CLEANUP BLOWDOWN ISOLATION VALVES SEEING 1050psid INSTEAD OF | | SEEING 140psid. | | | | A PRELIMINARY REVIEW OF DATA OBTAINED FROM TROUBLESHOOTING OF CONTAINMENT | | ISOLATION VALVES G33-F028 AND G33-F034 (RWCU BLOWDOWN ISOLATION VALVES) | | INDICATES THAT THE VALVES ARE SEEING A DIFFERENTIAL PRESSURE OF 1050psid, | | NOT THE 140psid DIFFERENTIAL PRESSURE THE VALVE TORQUE SWITCHES ARE | | CURRENTLY ADJUSTED TO, WHICH WAS THE ORIGINAL WORSE CASE DESIGN PRESSURE. | | GENERIC LETTER 89-10 TESTING ASSUMES WORST CASE CONDITIONS (1050psid). THE | | CONTAINMENT PENETRATION IS CURRENTLY ISOLATED AND BOTH VALVES ARE CLOSED. | | ENGINEERING EVALUATION IS STILL IN PROGRESS AND THEY ARE THINKING ABOUT | | POSSIBLY INCREASING THE TORQUE SETTING OF RWCU BLOWDOWN ISOLATION VALVES. | | | | RESIDENT INSPECTOR WAS INFORMED BY THE LICENSEE. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 28468 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: MILLSTONE REGION: 1 |NOTIFICATION DATE: 03/02/95 | |UNIT: [ ] [2] [ ] STATE: CT |NOTIFICATION TIME: 18:41 [ET]| |RX TYPE: [1] GE-3,[2] CE,[3] W-4-LP |EVENT DATE: 03/02/95 | +------------------------------------------------+EVENT TIME: 18:20[EST]| |NRC NOTIFIED BY: BAIN |LAST UPDATE DATE: 03/02/95 | |HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |HAROLD GRAY RDO | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | | | 2 | N N 0 REFUELING | 0 REFUELING | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CURRENT ABNORMAL OPERATING PROCEDURE PERMITS TWO SERVICE WATER PUMPS TO BE | | ELECTRICALLY ALIGNED TO THE SAME VITAL POWER FACILITY. | | | | DURING REVIEW OF ABNORMAL OPERATING PROCEDURES, A PROCEDURE WAS FOUND THAT | | WOULD ALLOW TWO SERVICE WATER PUMPS TO BE ELECTRICALLY ALIGNED TO THE SAME | | VITAL POWER FACILITY. UPON A LOSS OF NORMAL POWER, THIS CONDITION COULD | | RESULT IN THE SIMULTANEOUS START OF BOTH SERVICE WATER PUMPS (WHICH IS AN | | UNANALYZED CONDITION) THAT COULD CAUSE FAILURE OF THE OPERATING EMERGENCY | | DIESEL GENERATOR. LICENSEE IS INVESTIGATING THIS PROBLEM. | | | | RESIDENT INSPECTOR WAS INFORMED BY THE LICENSEE. | +------------------------------------------------------------------------------+ +----------------------------------+ +-----------------------+ |POWER REACTOR | |EVENT NUMBER: 28469 | +----------------------------------+ +-----------------------+ +------------------------------------------------+-----------------------------+ |FACILITY: PALISADES REGION: 3 |NOTIFICATION DATE: 03/02/95 | |UNIT: [1] [ ] [ ] STATE: MI |NOTIFICATION TIME: 22:40 [ET]| |RX TYPE: [1] CE |EVENT DATE: 03/02/95 | +------------------------------------------------+EVENT TIME: 20:09[EST]| |NRC NOTIFIED BY: V MOCERI |LAST UPDATE DATE: 03/02/95 | |HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+ NOTIFICATIONS | |EMERGENCY CLASS: NOT APPLICABLE +-----------------------------+ |10 CFR SECTION: |MCCORMICKBARGER RDO | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | | | | +-----+----------+-------+--------+--------------+--+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | 1 | N Y 100 POWER OPERATION | 91 POWER OPERATION | | | | | | | | | +-----+---------------------------------------------+--------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SPURIOUS ACTUATION OF THE LEFT CHANNEL LOAD SEQUENCER CAUSES SEVERAL | | ENGINEERED SAFEGUARDS SYSTEMS (ASSOCIATED WITH THE LEFT CHANNEL ONLY) TO | | ACTUATE. | | SPURIOUS ACTUATION OF THE LEFT CHANNEL LOAD SEQUENCER CAUSED THE FOLLOWING | | EQUIPMENT TO ACTUATE: HIGH PRESSURE SAFETY INJECTION PUMP (P-66B) STARTED, | | LOW PRESSURE SAFETY INJECTION PUMP (P-67B) STARTED, BORIC ACID PUMP | | STARTED, SERVICE WATER PUMP STARTED, VOLUME CONTROL TANK OUTLET VALVE | | CLOSED, BORIC ACID GRAVITY FEED VALVES OPENED (MO-2169 & 2170), LOW | | PRESSURE SAFETY INJECTION LOOP VALVES OPENED, & HIGH HEAD SAFETY INJECTION | | LOOP ISOLATION VALVES OPENED. THERE WAS NO INJECTION INTO THE REACTOR | | COOLANT SYSTEM SINCE REACTOR COOLANT SYSTEM PRESSURE WAS AT 2069psig AND | | THE HIGH HEAD SAFETY INJECTION PUMP DISCHARGE PRESSURE IS 1205psig. SAFETY | | INJECTION PUMPS RAN FOR APPROXIMATELY SEVEN MINUTES BEFORE THEY WERE | | SECURED. AFTER SECURING THE GRAVITY FEED VALVES LICENSEE HAD BORIC ACID IN | | THE CHARGING LINE. LICENSEE CONTROLLED THE INJECTION OF THE BORIC ACID IN | | THE CHARGING LINE TO THE REACTOR COOLANT SYSTEM. AS A RESULT OF THE | | INJECTION OF THE BORIC ACID INTO THE REACTOR COOLANT SYSTEM REACTOR POWER | | DECREASED TO 91%. REACTOR POWER HAS BEEN STABILIZED AT 91% AND WILL BE | | RETURNED TO 100%. LICENSEE IS INVESTIGATING WHY THE LEFT LOAD SEQUENCER | | ACTUATED. ALL SYSTEMS WERE RESTORED TO THEIR NORMAL LINEUP WITHIN 30 | | MINUTES AFTER THE SPURIOUS ACTUATION SIGNAL. | | EMERGENCY DIESEL GENERATOR (EDG 1-1) ASSOCIATED WITH THE LEFT LOAD | | SEQUENCER HAS BEEN DECLARED INOPERABLE WHICH PLACES PLANT IN TECH SPEC | | 3.7.2.I (SEVEN DAYS TO GET EDG 1-1 BACK OR SHUTDOWN). EMERGENCY DIESEL | | GENERATOR 1-2 IS FULLY OPERABLE IF NEEDED. EMERGENCY DIESEL GENERATOR 1-1 | | DID START BECAUSE OF THE SPURIOUS SIGNAL. ALL OTHER SAFETY SYSTEMS ARE | | CONSIDERED FULLY OPERABLE IF NEEDED. | | RESIDENT INSPECTOR WAS INFORMED BY THE LICENSEE. | +------------------------------------------------------------------------------+