Headquarters Daily Report AUGUST 12, 1998 *************************************************************************** REPORT NEGATIVE NO INPUT ATTACHED INPUT RECEIVED RECEIVED HEADQUARTERS û REGION I û REGION II û REGION III û REGION IV û PRIORITY ATTENTION REQUIRED MORNING REPORT - HEADQUARTERS AUGUST 12, 1998 MR Number: H-98-0122 NRR DAILY REPORT ITEM GENERIC COMMUNICATIONS Information Notice 98-30, "EFFECT OF YEAR 2000 COMPUTER PROBLEM ON NRC LICENSEES AND CERTIFICATE HOLDERS," will be issued on August 12, 1998. This notice is being issued to all material and fuel cycle licensees and certificate holders to remind them of the potential problems their computer systems and software may encounter as a result of the change to the year 2000. Addressees are encouraged to establish year 2000 readiness programs. Contact: Gary Purdy, NMSS 301-415-7897 E-mail: gwp1@nrc.gov _ REGION I MORNING REPORT PAGE 2 AUGUST 12, 1998 Licensee/Facility: Notification: Duquesne Light Co. MR Number: 1-98-0041 Beaver Valley 1 Date: 08/12/98 Shippingport,Pennsylvania SRI/PC Dockets: 50-334 PWR/W-3-LP Subject: UNIT RESTART AND REACTOR TRIP FOLLOWING EXTENDED FORCE OUTAGE Reportable Event Number: 34629 Discussion: On August 11, at 1:13 pm, the Unit 1 reactor was synchronized to the grid following completion of a 192 day forced outage. During the outage the licensee corrected various Technical Specifications surveillance test program weaknesses and design deficiencies. At 3:12 pm, the reactor tripped from 24 percent reactor power, due to an "A" steam generator (SG) steam flow/feedwater flow mismatch coincident with low SG level reactor protection signal. Shortly prior to the trip, the bistables for one channel of the "A" SG flow mismatch circuit had been placed in trip, in response to a failed steam flow channel. The "A" SG experienced a level transient while transferring feedwater flow control from the bypass feedwater regulating valve (FRV) to the main FRV. The normal SG level band during reactor startup is 28 percent to 38 percent narrow range level. Level reached the coincident 25 percent low SG level trip setpoint during the transfer, and the reactor tripped as designed. The plant responded to the trip as designed. The steam flow channel has been repaired and minor adjustments to the feedwater control system are in progress. The licensee has not announced a restart schedule, but restart is expected within the next few days. Contact: Neil Perry (610)337-5225 Dave Kern (412)643-2000 _