Headquarters Daily Report AUGUST 18, 1997 *************************************************************************** REPORT NEGATIVE NO INPUT ATTACHED INPUT RECEIVED RECEIVED HEADQUARTERS û REGION I û REGION II û REGION III û REGION IV û PRIORITY ATTENTION REQUIRED MORNING REPORT - REGION I AUGUST 18, 1997 Licensee/Facility: Notification: Connecticut Yankee Atomic Power Co. MR Number: 1-97-0045 Haddam Neck 1 Date: 08/18/97 Hartford,Connecticut Telephone 8/17/97 SRI Dockets: 50-213 PWR/W-4-LP Subject: TEMPORARY LOSS OF SPENT FUEL POOL COOLING Discussion: With the plant permanently shutdown for decommissioning and the reactor defueled, a lightning strike at the station at 2:07 a.m. on 8/17/97 caused the loss of spent fuel pool cooling and tripped several plant components. The plant equipment affected included the trip of the operating A spent fuel pool (SFP) cooling system pump, the temporary loss of the plant computer and security lighting, the tripping of several ventilation system fans (control room, switchgear room, spent fuel building, turbine building, administration building), and the tripping of the operating A service air compressor and the sample pumps for stack high range monitor RM-14B. The security diesel generator started and assumed loads. The plant emergency diesels did not start and were not required since there was no loss of the 4KV or 480 volt emergency buses. Plant operators and security personnel responded to the event using abnormal and emergency response procedures to identify offnormal equipment conditions and to restore normal equipment operation. An undervoltage (uv) lockout relay tripped and caused the isolation of service water to the SFP cooling system. The plant computer was restarted and functional by 2:21 a.m. Operators restarted the A SFP cooling pump, reset the timed relay, and restored cooling to the SFP by 2:25 a.m. SFP temperature remained stable at about 100 degrees F. The operators reviewed plant equipment conditions and restored equipment affected by the voltage transient. Plant electricians assisted in a systematic review of all electrical buses and panels. No equipment damage was identified. All equipment affected by the transient was restored. Licensee long term review and followup of the event was in progress as of August 18. Regional Action: The SRI responded to the site to verify plant status and review licensee actions. Region I will follow the licensee's event response. This information is current as of 8:00 a.m. on August 18. Contact: W. Raymond (860)267-2571 E. Conner (610)337-5399 _