Headquarters Daily Report AUGUST 19, 1996 *************************************************************************** REPORT NEGATIVE NO INPUT ATTACHED INPUT RECEIVED RECEIVED HEADQUARTERS û REGION I û REGION II û REGION III û REGION IV û PRIORITY ATTENTION REQUIRED MORNING REPORT - HEADQUARTERS AUGUST 19, 1996 MR Number: H-96-0063 NRR DAILY REPORT ITEM GENERIC COMMUNICATIONS NRC Information Notice 96-48, "Motor-Operated Valve Performance Issues," dated August 21, 1996. The NRC is issuing this information notice to alert addressees to (1) lessons learned from the Electric Power Research Institute Motor-Operated Valve (MOV) Performance Prediction Program, (2) performance problems with MOV key failures described in a recent NRC Office for Analysis and Evaluation of Operation Data study, and (3) the potential for torque output from MOV actuators to be less than predicted by Limitorque Corporation. Technical contacts: Thomas G. Scarbrough, NRR Chuck Hsu, AEOD (301) 415-2794 (301) 415-6356 Michael T. Bugg, RIII (630) 829-9500 _ REGION III MORNING REPORT PAGE 2 AUGUST 19, 1996 Licensee/Facility: Notification: Commonwealth Edison Co. MR Number: 3-96-0087 Zion 1 Date: 08/18/96 Zion,Illinois SRI VIA PC Dockets: 50-295 PWR/W-4-LP Subject: TURBINE TRIP AND REACTOR TRIP DUE TO LOW LEVEL IN THE "D" STEAM GENERATOR Discussion: On August 18, 1996, at 1133 hours (CDT), Unit 1 tripped on low steam generator level when the 1D MSIV partially closed during quarterly surveillance testing. Steam generator level shrunk to less than the low-low steam generator water level reactor trip setpoint which caused a reactor trip and a subsequent turbine trip. All equipment performed as expected with two exceptions. The rod bottom lights for the D-4 and C-11 control rods came in slow and there was slow response by pressurizer level controller, 1LR-459. The slow rod bottom lights for control rods D-14 and C-11 were subsequently determined to be a problem with the rod position indication system. During the trip transient, pressure surges in the Unit 1 heater drain tank (HDT) caused its rupture disk to rupture. The 1D MSIV test failure was determined to be a failed NAMCO limit switch. The licensee is currently inspecting the other three MSIV NAMCO limit switches. The licensee is working on the HDT rupture disk replacement and plans to restart the unit Tuesday evening. Regional Action: The resident staff are continuing to followup the licensee's investigation and assessment of equipment failures. Contact: L.F. MILLER, JR. (630)829-9629 _ REGION III MORNING REPORT PAGE 3 AUGUST 19, 1996 Licensee/Facility: Notification: Commonwealth Edison Co. MR Number: 3-96-0088 Zion 1 2 Date: 08/19/96 Zion,Illinois SRI Dockets: 50-295,50-304 PWR/W-4-LP,PWR/W-4-LP Subject: OVERFLOW OF LAKE DISCHARGE TANK (LDT) Discussion: On Friday, Aug 16, 1996, at 8:30 p.m. (CDT) approximately 7000 gallons of slightly contaminated water overflowed from the OB lake discharge tank (LDT) to the auxiliary building (AB) floor. When an LDT overflows, it is hard piped to a 200 gal sump. When the sump is full, it causes the floor drains to backup. The overflow was caused by an operator's inattention to detail by failure to close the lake discharge tank inlet isolation valve 0WD- 0118. Regional Action: The resident staff is continuing to followup the licensee's investigation and assessment of the incident. Contact: L.F. MILLER, JR. (630)829-9629 _