Headquarters Daily report JUNE 13, 1994 *************************************************************************** REPORT NEGATIVE NO INPUT ATTACHED INPUT RECEIVED RECEIVED HEADQUARTERS X REGION I X REGION II X REGION III X REGION IV X *************************************************************************** PRIORITY ATTENTION REQUIRED MORNING REPORT - REGION IV JUNE 13, 1994 Licensee/Facility: Notification: Entergy Operations, Inc. MR Number: 4-94-0053 Waterford 3 Date: 06/13/94 Killona,Louisiana SRI Dockets: 50-382 PWR/CE Subject: INADVERTENT REACTOR CUTBACK Reportable Event Number: N/A Discussion: On June 12, 1994, at 11 a.m., while operating at full power, the Waterford-3 plant experienced a reactor cutback due to a turbine trip. (The reactor cutback automatically inserts preselected control element assembly Subgroups 5 and 11 into the core.) The turbine trip occurred when a moisture separator reheater (MSR) high water level was received. The plant was stabilized at approximately 20 percent power utilizing the steam bypass system. All reactor cutback functions occurred as designed and no abnormal cutback system responses were observed by the licensee. The operators maintained the plant at that power level while troubleshooting efforts commenced to determine the cause of the problem. Plant management convened an Event Review Team (ERT) to perform a root cause analysis prior to returning the plant to full power. The ERT initial results indicated that one of three level indicators on an MSR sensed a high level and its mercury switch stuck in the high level position. While operators were evaluating the resultant annunciator, a second high level on that MSR was received and completed the coincidence needed for a turbine trip. The ERT determined that the root cause of the event was equipment malfunction due to lack of insulation on the common high point sensing line for the instruments. The lack of insulation apparently allowed steam condensation in the line when heavy thunderstorm activity in the area caused a sudden drop in temperature. Additionally, the ERT reported that thunderstorm-induced vibrations resulted in the level switch actuation. The licensee is evaluating the adequacy of present piping supports to prevent inadvertent actuation of the MSR level switches due to vibration and that all level switches are free to actuate and reset. As of 8 a.m., on June 13 the plant was at 30 percent power while holding for condenser chemistry to come into specification. The licensee intends to return to full power operations upon satisfying chemistry requirements. Regional Action: The SRI was onsite at the time of the event and responded to the control room to observe activities and evaluate the event. Regional management was telephonically informed of the plant status. Contact: Chris Vandenburgh (817)860-8161